改进有效的支撑和压裂技术是低渗透低煤阶煤层气储层增产成功的关键

Xin Wang, Qingzhong Zhu, Wei Zheng, H. Lu
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引用次数: 1

摘要

中国具有丰富的低煤阶煤层气资源。研究对象为二连盆地吉尔嘎朗图凹陷低阶褐煤煤层。储层低孔低渗,无天然产能。煤层埋深200 ~ 600 m,煤层厚度40 ~ 60 m, Ro值为0.32% ~ 0.47%。借鉴该地区常规低阶煤层完井经验思路,两口井采用裸眼空腔完井技术,产量仅为150 m3/d左右。在另一口井进行了常规活水压裂试验,压裂后产量为200-300 m3/d。增产效果很差,限制了该地区的商业开发活动。通过对两口井的应用,介绍了水力爆破注浆崩落压裂技术和反向复合压裂技术两种通过提高煤层诱导裂缝扩展和支护能力来提高增产效果的技术。压裂后的恒定产量达到1500 ~ 2000 m3/d,远高于经济开发下限600m3/d。得到了令人振奋的结果。这些技术的探索对低煤阶煤层气增产具有重要意义,可以帮助我们在低煤阶煤层实施有效的压裂增产作业,获得最佳的生产效果。
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Improving the Effective Supporting and Fracturing Technology is the Key to the Successful Stimulation of Low-Permeability and Low-Rank Coalbed Methane Reservoirs
China has abundant low-rank coalbed methane resources. The research object is the low rank lignite seams in Jiergalangtu Sag in Erlian Basin. The reservoir has low porosity and low permeability, and it has no natural productivity. The coal seams have a burial depth of 200-600 meters, thickness of 40-60 meters, and Ro of 0.32% to 0.47%. Borrowing the idea of well completion experience for the conventional low rank coal seams in the region, open hole cavity completion techniques were adopted in two wells, obtaining an output of only about 150 m3/d. The conventional active water fracturing was also tested in another well, and the output after fracturing was 200-300 m3/d. The effect of stimulation was very poor, which limited commercial exploitation activities in the region. This paper introduces two techniques to improve the effect of stimulation by improving induced fracture extension and supporting capacity in the coal seams, including the hydraulic blasting & grouting caving fracturing technique and the reverse compound fracturing technique, which were applied in two wells. A constant rate of production after fracturing reached 1,500-2,000m3/d, which was well above the lower limit output of economic exploitation in the region of 600m3/d. Exciting results were obtained. The exploration of these techniques is of great significance for low rank coalbed methane stimulation, which can help us to implement effective fracturing stimulation operation in low rank coal seams to obtain the best production effect.
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