高温高压致密气藏多级压裂井再射孔提高产能的实例研究

Ryosuke Kidogawa, N. Yoshida, K. Fuse, Yuta Morimoto, K. Takatsu, Keisuke Yamamura
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引用次数: 0

摘要

在长期生产过程中,多级压裂气井的产能可能会因导流能力受损和非达西流动而降低。这种退化现象在射孔段较短的井段中表现得尤为明显,而识别退化段进行修复则是一项挑战。此外,在高压和高温(HP/HT)环境下,补救措施的成本很高。一个现场案例表明,通过优先考虑具有多速率生产测井(PL)结果的目标,重新射孔作为一种经济有效的方法,成功地缓解了流体收敛。本研究通过数值模拟和对日本陆上高温高压火山岩气藏一口六段压裂井的再射孔进行了理论研究。在超过15年的生产过程中,人们怀疑明显的导电性降低,并通过与短射孔段的流动收敛相关的非达西流动效应来证明。在瞬态后流测试中,通过量化各级的流入动态关系(IPR),采用多速率PL识别受损级。受损的压裂段使用电缆输送射孔器重新射孔,增加射孔间隔。使用前/后压力累积测试和工作后PL来验证生产率的提高。根据多速率PL的结果,确定了再射孔的目标区域,并对其进行了优先排序。绘制了阶段的ipr,通过ipr的形状和/或随着地面速率的增加流入贡献的减少,在三个阶段中确定了相对较大的非达西效应。温度测井结果显示,第四阶段底部温度变化剧烈;裂缝可能在射孔段下方扩展。根据估计的阶段知识产权校准的数值模型估计了生产增量的范围。根据计划的再射孔方案,预计增产幅度在15%至30%之间,而增产幅度则取决于新射孔与现有裂缝之间的连接。随后,进行了重新射孔作业,经过一个月的生产,在井口压力不变的情况下,气产率提高了26%。再射孔后3个月进行作业后PL。井的IPR得到了改善,这意味着非达西效应的降低。压力累积试验的结果也表明皮肤因子减少。根据作业后的PL重新绘制了段段ip,结果表明,在压裂过程中发生筛出的两个段和怀疑存在明显非达西效应的一个段,都有明显的改进。本文提出的工作流程和策略可用于在长期生产中具有短射孔段和表观导流能力下降的多级压裂气井,以经济有效的方式恢复产能。特别是,解释结果表明,在压裂过程中发生筛出的阶段,所提出的方法可以有效地提高产能。此外,我们还讨论了对PL进行仔细测试设计的重要性,因为它们是成功的关键。
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Productivity Improvement by Re-perforation of Multistage-fractured Wells in HP/HT Tight Gas Reservoirs: A Case History
Productivity of multistage-fractured gas wells is possibly degraded by conductivity impairments and non-Darcy flow during long-term production. Such degradations are pronounced by flow convergence to short perforated intervals, while it is challenging to identify degraded stages for remediation. Moreover, remedial actions can be expensive under high-pressure and high-temperature (HP/HT) environment. A field case demonstrates successful application of re-perforation as a cost-effective way to mitigate the flow convergence by prioritizing targets with multi-rate production logging (PL) results. This work presents theoretical investigations using numerical simulations and field execution of re-perforation for a well with six-stage fracturing treatments in a HP/HT volcanic gas reservoir onshore Japan. Apparent conductivity reduction was suspected during more than 15 years of production, and it was pronounced by non-Darcy flow effects associated with flow convergence to short perforated intervals. Multi-rate PL was employed to identify impaired stages by quantifying inflow performance relationship (IPR) of each stage under transient flow-after-flow testing. The impaired stages were re-perforated adding perforation intervals with wireline-conveyed perforators. Pre/post pressure build-up tests and post-job PL were used to validate productivity improvements. Target zones for re-perforations were identified and prioritized with results of the multi-rate PL conducted. The stage IPRs were drawn, and relatively large non-Darcy effects were identified in three stages by shapes of the IPRs and/or decreasing inflow contributions as surface rate increased. Also, temperature log showed steep temperature change at bottom of the 4th stage; the fracture might propagate below the perforated interval. Ranges of production increment were estimated using a numerical model calibrated against the estimated stage IPRs. The estimated increment was in range of 15% to 30% with planned re-perforation program while its magnitude depended on connection between new perforations and existing fractures. Afterwards, re-perforation job was done, and, the gas rate was confirmed to be increased by 26% with the same well-head pressure after one month of production. The post-job PL was conducted three months after the re-perforation. The well's IPR was improved implying reduction of the non-Darcy effects. Results of pressure build-up tests also indicated reduction of skin factor. The stage IPRs were redrawn with the post-job PL, and they suggested clear improvements in two stages where screen-out occurred during fracturing treatments and a stage where significant non-Darcy effect was suspected. The workflow and strategy in this paper can be applied for productivity restoration in a cost-effective way to multi-stage fractured gas wells with short perforated intervals and impaired apparent conductivity during long-term production. Especially, the interpreted results suggested effectiveness of the proposed approach for productivity improvement in stages where screenout occurs during fracturing treatments. Moreover, lessons learned on importance of careful test designs for PL were discussed because they are keys for success.
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