为提高工作位置和生产率而重新设计的方形木材砂光机(以Abu Production handcraft为例,Pleret, Bantul, Yogyakarta)

Kristanto Agung, Saputra Agung
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引用次数: 1

摘要

Abu Production Handycraft是一家中小型企业,生产各种类型的工艺品,如纸巾盒、灯杯、烟灰缸、果篮、花盆、花瓶、牌匾、托盘、纪念品和其他类型的木制工艺品。其中一个生产过程是砂化过程,该过程是由操作员长时间坐在小工作台上进行的。它导致工人工作时背部弯曲,低头,手肘和双腿包括膝盖折叠。标准化北欧问卷(SNQ)显示,该员工的颈部、肩部、肘部、手腕、背部、臀部和膝盖疼痛。因此,这可能会影响工作效率。本研究的目的是重新设计方型材木材砂磨机,以提高工作位置和生产率。将人机工程学的概念应用于工作设施的设计。在本研究中,通过测量被试的不适感、标准时间和工作效率来比较重新设计前后的条件。以人体测量数据为参考,设计与工人身体尺寸相匹配的砂光机尺寸。本研究采用SolidWorks软件对砂光机进行设计。结果显示,不适程度从70%下降到10%。在标准用时方面,初始用时为20.96分钟/单位,最终用时为7.99分钟/单位。与标准时间相比,下降了61.88%。与标准输出相关,它显示初始条件为3.00单位/分钟,最终条件为8.00单位/分钟。结果表明,与初始条件相比,生产效率提高了166.67%。
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Redesign of Squared-Profile Wood Sanding Machine for Work-Position and Productivity Improvement (Case study on Abu Production Handycraft, Pleret, Bantul, Yogyakarta)
Abu Production Handycraft was a small and medium enterprise (SME) that produced various types of handicraft products, such as tissue boxes, lamp cups, ashtrays, fruit baskets, flowerpots, flower vases, plaques, trays, souvenirs, and other types of wooden craft product. One of production processes was sanding process which was performed by the operator while in sitting position on a small bench for long time. It caused the worker worked with the back in bent position, head bowed, elbows and both legs include knees folded. Standardised Nordic Questionnaires (SNQ) revealed that the worker suffered from pain in the neck, shoulder, elbow, wrist, back, buttock, and knee. So, it could effect on the work productivity. The objective of this research was to redesign of squared-profile wood sanding machine for Work-position and Productivity Improvement. The concept of ergonomics was applied for work facilities designing. The discomfort perceived, standard time, and work productivity would be measured for comparing between pre and post redesigning conditions on this research. The anthropometric data was taken as reference for the dimension of sanding machine design which matched to the body dimension of the worker. SolidWorks software was used in this research for sanding machine designing. The result showed a decrease on the level of discomfort of 70% into 10%. Regarding to the standard time, the result showed 20.96 minutes/unit and 7.99 minutes/unit for initial and final condition, respectively. It indicated a decrease of 61.88% in term of standard time. Related to the standard output, it showed 3.00 units/minute for initial condition and 8.00 units/minute for final condition. It indicated that there was an increase of 166.67% in term of productivity when compared to the initial condition.
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