A. Gadelhak, Mohamed Al-Badi, Ahmed Al-Bairaq, E. Al Mheiri, Abdullah Haj Al-Hosani, Z. Ahmed, Sami Ullah Bashir Ahmed, Mubashir Ahmed, Waleed Omar Abedelkhalik, Sameh Hassan Naser, Haysam El-Shater, Wessam Al Assar, Steve Ross, Blair Duncan
{"title":"通过使用跨式封隔器,将应用程序导向固液井,成功案例","authors":"A. Gadelhak, Mohamed Al-Badi, Ahmed Al-Bairaq, E. Al Mheiri, Abdullah Haj Al-Hosani, Z. Ahmed, Sami Ullah Bashir Ahmed, Mubashir Ahmed, Waleed Omar Abedelkhalik, Sameh Hassan Naser, Haysam El-Shater, Wessam Al Assar, Steve Ross, Blair Duncan","doi":"10.2118/207840-ms","DOIUrl":null,"url":null,"abstract":"\n \n \n The Increase of inactive wells due to subsurface integrity issue is observed in brown fields, Fig-1 is, showing the record for onshore UAE asset, the economic challenges is calling for alternative solutions to restore well integrity with lower cost.\n Straddle packer application is consists of two tandom packers with spacer pipe in between with anchoring system deployed riglessly in the well to isolate the communication point between Ann A and Tubing.Fig-2,\n \n \n \n Communication between tubing and annulus A (Failure of primary barrier) is identified as the right candidate wells for straddle packer application,\n First step is to clearly identify the point of communication, it has been done by annulus pressure investigation excersize during flowing and shut in condition, observing the return of annulus fluid which was the same produced gas\n Noise log has been conducted and clearly identified the communication point at SPM (Side Pocket Mandrel) to be used for emergency killing,\n Tubing integrity test was conducted using nippless plugs and inflow test below and above the leak point and confirm no other leak points within the tubing\n Engineering drawing for the leaking assembly was reviewed to design the dimension of straddle packer assembly, length and packer size\n It is recommended to deploy the assembly using electric line correlation for accurate depth selection\n After setting annulus pressure observed no build up\n Well opened safely to production\n \n \n \n Leak point arrested, well primary barrier restored\n Removed from DWS (drilling and workover schedule) and restore well production in addition to improving inactive string KPI for Gas asset\n Save almost work over cost for gas well XX-197\n \n \n \n The way forward is to check the scalability of extending this application among other ADNOC assets and to screen the right candidate wells for this application\n To add this application as a part of well integrity procedures and recommendations for such like cases\n","PeriodicalId":11069,"journal":{"name":"Day 2 Tue, November 16, 2021","volume":"13 1","pages":""},"PeriodicalIF":0.0000,"publicationDate":"2021-12-09","publicationTypes":"Journal Article","fieldsOfStudy":null,"isOpenAccess":false,"openAccessPdf":"","citationCount":"0","resultStr":"{\"title\":\"Lead Application to Cure Sap Wells by Deploying Straddle Packer, Success Story\",\"authors\":\"A. Gadelhak, Mohamed Al-Badi, Ahmed Al-Bairaq, E. Al Mheiri, Abdullah Haj Al-Hosani, Z. Ahmed, Sami Ullah Bashir Ahmed, Mubashir Ahmed, Waleed Omar Abedelkhalik, Sameh Hassan Naser, Haysam El-Shater, Wessam Al Assar, Steve Ross, Blair Duncan\",\"doi\":\"10.2118/207840-ms\",\"DOIUrl\":null,\"url\":null,\"abstract\":\"\\n \\n \\n The Increase of inactive wells due to subsurface integrity issue is observed in brown fields, Fig-1 is, showing the record for onshore UAE asset, the economic challenges is calling for alternative solutions to restore well integrity with lower cost.\\n Straddle packer application is consists of two tandom packers with spacer pipe in between with anchoring system deployed riglessly in the well to isolate the communication point between Ann A and Tubing.Fig-2,\\n \\n \\n \\n Communication between tubing and annulus A (Failure of primary barrier) is identified as the right candidate wells for straddle packer application,\\n First step is to clearly identify the point of communication, it has been done by annulus pressure investigation excersize during flowing and shut in condition, observing the return of annulus fluid which was the same produced gas\\n Noise log has been conducted and clearly identified the communication point at SPM (Side Pocket Mandrel) to be used for emergency killing,\\n Tubing integrity test was conducted using nippless plugs and inflow test below and above the leak point and confirm no other leak points within the tubing\\n Engineering drawing for the leaking assembly was reviewed to design the dimension of straddle packer assembly, length and packer size\\n It is recommended to deploy the assembly using electric line correlation for accurate depth selection\\n After setting annulus pressure observed no build up\\n Well opened safely to production\\n \\n \\n \\n Leak point arrested, well primary barrier restored\\n Removed from DWS (drilling and workover schedule) and restore well production in addition to improving inactive string KPI for Gas asset\\n Save almost work over cost for gas well XX-197\\n \\n \\n \\n The way forward is to check the scalability of extending this application among other ADNOC assets and to screen the right candidate wells for this application\\n To add this application as a part of well integrity procedures and recommendations for such like cases\\n\",\"PeriodicalId\":11069,\"journal\":{\"name\":\"Day 2 Tue, November 16, 2021\",\"volume\":\"13 1\",\"pages\":\"\"},\"PeriodicalIF\":0.0000,\"publicationDate\":\"2021-12-09\",\"publicationTypes\":\"Journal Article\",\"fieldsOfStudy\":null,\"isOpenAccess\":false,\"openAccessPdf\":\"\",\"citationCount\":\"0\",\"resultStr\":null,\"platform\":\"Semanticscholar\",\"paperid\":null,\"PeriodicalName\":\"Day 2 Tue, November 16, 2021\",\"FirstCategoryId\":\"1085\",\"ListUrlMain\":\"https://doi.org/10.2118/207840-ms\",\"RegionNum\":0,\"RegionCategory\":null,\"ArticlePicture\":[],\"TitleCN\":null,\"AbstractTextCN\":null,\"PMCID\":null,\"EPubDate\":\"\",\"PubModel\":\"\",\"JCR\":\"\",\"JCRName\":\"\",\"Score\":null,\"Total\":0}","platform":"Semanticscholar","paperid":null,"PeriodicalName":"Day 2 Tue, November 16, 2021","FirstCategoryId":"1085","ListUrlMain":"https://doi.org/10.2118/207840-ms","RegionNum":0,"RegionCategory":null,"ArticlePicture":[],"TitleCN":null,"AbstractTextCN":null,"PMCID":null,"EPubDate":"","PubModel":"","JCR":"","JCRName":"","Score":null,"Total":0}
Lead Application to Cure Sap Wells by Deploying Straddle Packer, Success Story
The Increase of inactive wells due to subsurface integrity issue is observed in brown fields, Fig-1 is, showing the record for onshore UAE asset, the economic challenges is calling for alternative solutions to restore well integrity with lower cost.
Straddle packer application is consists of two tandom packers with spacer pipe in between with anchoring system deployed riglessly in the well to isolate the communication point between Ann A and Tubing.Fig-2,
Communication between tubing and annulus A (Failure of primary barrier) is identified as the right candidate wells for straddle packer application,
First step is to clearly identify the point of communication, it has been done by annulus pressure investigation excersize during flowing and shut in condition, observing the return of annulus fluid which was the same produced gas
Noise log has been conducted and clearly identified the communication point at SPM (Side Pocket Mandrel) to be used for emergency killing,
Tubing integrity test was conducted using nippless plugs and inflow test below and above the leak point and confirm no other leak points within the tubing
Engineering drawing for the leaking assembly was reviewed to design the dimension of straddle packer assembly, length and packer size
It is recommended to deploy the assembly using electric line correlation for accurate depth selection
After setting annulus pressure observed no build up
Well opened safely to production
Leak point arrested, well primary barrier restored
Removed from DWS (drilling and workover schedule) and restore well production in addition to improving inactive string KPI for Gas asset
Save almost work over cost for gas well XX-197
The way forward is to check the scalability of extending this application among other ADNOC assets and to screen the right candidate wells for this application
To add this application as a part of well integrity procedures and recommendations for such like cases