基于内部液压位置反馈的两级比例阀性能改进研究

IF 1.7 4区 计算机科学 Q3 AUTOMATION & CONTROL SYSTEMS Journal of Dynamic Systems Measurement and Control-Transactions of the Asme Pub Date : 2021-07-01 DOI:10.1115/1.4049793
He Wang, Xiaohu Wang, Jiahai Huang, Long Quan
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引用次数: 4

摘要

本文研究了一种具有内部液压位置反馈的两级比例阀的性能改进,该阀被称为Valvistor阀。通过辨识该阀的性能约束,提出了一种基于积分-分离模糊比例-积分-微分控制器的电子闭环控制策略,以改善该阀的静态和动态性能。结果表明:在Valvistor阀中,内部液压位置反馈的比较点和反馈回路仅在主级,而输入则在先导级;这导致该阀门性能差。该控制策略非常有效,提高了Valvistor阀的性能。采用该控制策略,通过实时调节先导阶段阀芯位移,将导阀位移误差从4.9%降低到2.1%,流量误差从5.3%降低到2.3%。消除了锥筒位移和流量的死区。迟滞从5.3%降低到2.6%,线性度提高。超调量从0.06 mm减少到0.02 mm,沉降时间从0.5 s减少到0.2 s。带宽由8 Hz增加到16 Hz。
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Performance Improvement of a Two-Stage Proportional Valve With Internal Hydraulic Position Feedback
The present research concentrates on the performance improvement of a two-stage proportional valve with internal hydraulic position feedback which is named as the Valvistor valve. In this paper, the performance constraint of this valve is identified and a novel electronic closed-loop control strategy with an integral-separation fuzzy proportional-integral-derivative controller is proposed to improve the valve performance, including the static characteristics and the dynamic characteristics. The results show that in the Valvistor valve, the comparison point and the feedback loop for the internal hydraulic position feedback is only in the main stage, while the input is in the pilot stage. This leads to the poor performance of this valve. The control strategy is very effective and the performance of the Valvistor valve is improved. With the control strategy, the error of the poppet displacement is reduced from 4.9% to 2.1% by adjusting the spool displacement in the pilot stage in real-time and the flow error is reduced from 5.3% to 2.3%. The dead zone of the poppet displacement and the flow is eliminated. The hysteresis is reduced from 5.3% to 2.6% and the linearity is improved. The overshoot is reduced from 0.06 to 0.02 mm and the settling time is reduced from 0.5 to 0.2 s. Moreover, the bandwidth is increased from 8 to 16 Hz.
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来源期刊
CiteScore
3.90
自引率
11.80%
发文量
79
审稿时长
24.0 months
期刊介绍: The Journal of Dynamic Systems, Measurement, and Control publishes theoretical and applied original papers in the traditional areas implied by its name, as well as papers in interdisciplinary areas. Theoretical papers should present new theoretical developments and knowledge for controls of dynamical systems together with clear engineering motivation for the new theory. New theory or results that are only of mathematical interest without a clear engineering motivation or have a cursory relevance only are discouraged. "Application" is understood to include modeling, simulation of realistic systems, and corroboration of theory with emphasis on demonstrated practicality.
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