Eagle Ford东部的小规模EOR试验提高了产量

Tim Bozeman, W. Nelle, Q. Nguyen
{"title":"Eagle Ford东部的小规模EOR试验提高了产量","authors":"Tim Bozeman, W. Nelle, Q. Nguyen","doi":"10.2118/209429-ms","DOIUrl":null,"url":null,"abstract":"\n Low primary and secondary recoveries of original oil in place from modern unconventional reservoirs begs for utilization of tertiary recovery techniques. Enhanced Oil Recovery (EOR) via cyclic gas injection (\"huff ‘n puff\") has indeed enhanced oil recovery in many fields and many of those projects have also been documented in industry technical papers/case studies. But the need remains to document new techniques in new reservoirs. This paper documents a small scale EOR pilot project in the eastern Eagle Ford and shows promising well results.\n In preparation for the pilot, full characterization of the oil and injection gas was done along with laboratory testing to identify the miscibility properties of the two fluids. Once the injection well facility design was completed a series of progressively larger gas volumes were injected followed by correspondingly longer production times. Fluids in the returning liquid and gas streams were monitored for compositional changes and the learnings from each cycle led to adjustments and facility changes to improve the next cycle.\n After completing five injection/withdrawal cycles in the pilot a few key observations can be made. The implementation of cyclic gas injection can be both a technical and a commercial success early in its life if reasonable cost controls are implemented and the scope is kept manageable. The process has proved to be both repeatable and predictable allowing for economic modeling to be utilized to help determine timing of subsequent injection cycles. A key component of the success of this pilot has been the availability of small compressors capable of the high pressures required for these projects and learning how to implement cost saving facility designs that still meet high safety standards.","PeriodicalId":10935,"journal":{"name":"Day 1 Mon, April 25, 2022","volume":"30 1","pages":""},"PeriodicalIF":0.0000,"publicationDate":"2022-04-18","publicationTypes":"Journal Article","fieldsOfStudy":null,"isOpenAccess":false,"openAccessPdf":"","citationCount":"0","resultStr":"{\"title\":\"Small Scale EOR Pilot in the Eastern Eagle Ford Boosts Production\",\"authors\":\"Tim Bozeman, W. Nelle, Q. Nguyen\",\"doi\":\"10.2118/209429-ms\",\"DOIUrl\":null,\"url\":null,\"abstract\":\"\\n Low primary and secondary recoveries of original oil in place from modern unconventional reservoirs begs for utilization of tertiary recovery techniques. Enhanced Oil Recovery (EOR) via cyclic gas injection (\\\"huff ‘n puff\\\") has indeed enhanced oil recovery in many fields and many of those projects have also been documented in industry technical papers/case studies. But the need remains to document new techniques in new reservoirs. This paper documents a small scale EOR pilot project in the eastern Eagle Ford and shows promising well results.\\n In preparation for the pilot, full characterization of the oil and injection gas was done along with laboratory testing to identify the miscibility properties of the two fluids. Once the injection well facility design was completed a series of progressively larger gas volumes were injected followed by correspondingly longer production times. Fluids in the returning liquid and gas streams were monitored for compositional changes and the learnings from each cycle led to adjustments and facility changes to improve the next cycle.\\n After completing five injection/withdrawal cycles in the pilot a few key observations can be made. The implementation of cyclic gas injection can be both a technical and a commercial success early in its life if reasonable cost controls are implemented and the scope is kept manageable. The process has proved to be both repeatable and predictable allowing for economic modeling to be utilized to help determine timing of subsequent injection cycles. A key component of the success of this pilot has been the availability of small compressors capable of the high pressures required for these projects and learning how to implement cost saving facility designs that still meet high safety standards.\",\"PeriodicalId\":10935,\"journal\":{\"name\":\"Day 1 Mon, April 25, 2022\",\"volume\":\"30 1\",\"pages\":\"\"},\"PeriodicalIF\":0.0000,\"publicationDate\":\"2022-04-18\",\"publicationTypes\":\"Journal Article\",\"fieldsOfStudy\":null,\"isOpenAccess\":false,\"openAccessPdf\":\"\",\"citationCount\":\"0\",\"resultStr\":null,\"platform\":\"Semanticscholar\",\"paperid\":null,\"PeriodicalName\":\"Day 1 Mon, April 25, 2022\",\"FirstCategoryId\":\"1085\",\"ListUrlMain\":\"https://doi.org/10.2118/209429-ms\",\"RegionNum\":0,\"RegionCategory\":null,\"ArticlePicture\":[],\"TitleCN\":null,\"AbstractTextCN\":null,\"PMCID\":null,\"EPubDate\":\"\",\"PubModel\":\"\",\"JCR\":\"\",\"JCRName\":\"\",\"Score\":null,\"Total\":0}","platform":"Semanticscholar","paperid":null,"PeriodicalName":"Day 1 Mon, April 25, 2022","FirstCategoryId":"1085","ListUrlMain":"https://doi.org/10.2118/209429-ms","RegionNum":0,"RegionCategory":null,"ArticlePicture":[],"TitleCN":null,"AbstractTextCN":null,"PMCID":null,"EPubDate":"","PubModel":"","JCR":"","JCRName":"","Score":null,"Total":0}
引用次数: 0

摘要

现代非常规油藏原油一次采收率和二次采收率较低,需要采用三次采收率技术。通过循环注气(“huff”n puff”)提高采收率(EOR)确实在许多油田提高了采收率,其中许多项目也被记录在行业技术论文/案例研究中。但在新油藏中记录新技术的需求仍然存在。本文记录了Eagle Ford东部的一个小规模EOR试点项目,并显示出良好的效果。为了进行试验准备,对油气进行了全面表征,并进行了实验室测试,以确定两种流体的混相特性。一旦完成了注水井设施的设计,注入的气体量就会越来越大,相应的生产时间也会越来越长。对返回的液体和气体流中的流体进行了成分变化监测,并从每个循环中吸取教训,从而进行调整和设备更改,以改进下一个循环。在试验中完成五个注入/提取周期后,可以进行一些关键观察。如果实施合理的成本控制,并且范围保持在可控范围内,循环注气可以在其生命周期的早期取得技术和商业上的成功。事实证明,该过程具有可重复性和可预测性,可以利用经济建模来帮助确定后续注入周期的时间。该试点项目成功的一个关键因素是能够承受这些项目所需的高压的小型压缩机的可用性,以及学习如何在满足高安全标准的情况下实施节省成本的设施设计。
本文章由计算机程序翻译,如有差异,请以英文原文为准。
查看原文
分享 分享
微信好友 朋友圈 QQ好友 复制链接
本刊更多论文
Small Scale EOR Pilot in the Eastern Eagle Ford Boosts Production
Low primary and secondary recoveries of original oil in place from modern unconventional reservoirs begs for utilization of tertiary recovery techniques. Enhanced Oil Recovery (EOR) via cyclic gas injection ("huff ‘n puff") has indeed enhanced oil recovery in many fields and many of those projects have also been documented in industry technical papers/case studies. But the need remains to document new techniques in new reservoirs. This paper documents a small scale EOR pilot project in the eastern Eagle Ford and shows promising well results. In preparation for the pilot, full characterization of the oil and injection gas was done along with laboratory testing to identify the miscibility properties of the two fluids. Once the injection well facility design was completed a series of progressively larger gas volumes were injected followed by correspondingly longer production times. Fluids in the returning liquid and gas streams were monitored for compositional changes and the learnings from each cycle led to adjustments and facility changes to improve the next cycle. After completing five injection/withdrawal cycles in the pilot a few key observations can be made. The implementation of cyclic gas injection can be both a technical and a commercial success early in its life if reasonable cost controls are implemented and the scope is kept manageable. The process has proved to be both repeatable and predictable allowing for economic modeling to be utilized to help determine timing of subsequent injection cycles. A key component of the success of this pilot has been the availability of small compressors capable of the high pressures required for these projects and learning how to implement cost saving facility designs that still meet high safety standards.
求助全文
通过发布文献求助,成功后即可免费获取论文全文。 去求助
来源期刊
自引率
0.00%
发文量
0
期刊最新文献
Determination of Transmission Coefficient and Electric Field Distribution of Rice Husk/ Pcl Composites Using Finite Element Method for Microwave Devices Mechanical Properties Evaluation in Friction Stir Welding of Different Pipes The chemistry of aluminum salts in papermaking Comparative study of guar gum and its cationic derivatives as pre-flocculating polymers for PCC fillers in papermaking applications Ultrastructural behavior of cell wall polysaccharides
×
引用
GB/T 7714-2015
复制
MLA
复制
APA
复制
导出至
BibTeX EndNote RefMan NoteFirst NoteExpress
×
×
提示
您的信息不完整,为了账户安全,请先补充。
现在去补充
×
提示
您因"违规操作"
具体请查看互助需知
我知道了
×
提示
现在去查看 取消
×
提示
确定
0
微信
客服QQ
Book学术公众号 扫码关注我们
反馈
×
意见反馈
请填写您的意见或建议
请填写您的手机或邮箱
已复制链接
已复制链接
快去分享给好友吧!
我知道了
×
扫码分享
扫码分享
Book学术官方微信
Book学术文献互助
Book学术文献互助群
群 号:481959085
Book学术
文献互助 智能选刊 最新文献 互助须知 联系我们:info@booksci.cn
Book学术提供免费学术资源搜索服务,方便国内外学者检索中英文文献。致力于提供最便捷和优质的服务体验。
Copyright © 2023 Book学术 All rights reserved.
ghs 京公网安备 11010802042870号 京ICP备2023020795号-1