Applying DeviceNet in motor control centers at a cement plant

S. Simonye, L. Alpena, G. Witte
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引用次数: 1

Abstract

The Lafarge Cement Plant in Alpena, MI produces 2.5 million tons of cement per year from 5 kilns which each yield around 1250 tons per day. Plant control is distributed over forty PLC5s with over eighteen thousand I/O points, which have been installed over ten years. The kilns were the last major pieces of equipment yet to be tied into the PLC based supervisory system. PLC5s were chosen for the kiln automation based on this installed base and on the ease of expanding the existing supervisory system network to accommodate the kiln control. The plant architecture uses three layers of communication: first, remote I/O to communicate to the I/O subsystem from the PLC Processor; and secondly, a Data Highway Plus to communicate between processors and to the Ethernet gateway/data server. This gateway provides process data to the third layer, the process supervisory network. The process supervisory network consists of supervisory workstations running Intellution DMACs and the expert system LUCIE which is Lafarge's own application running on Gensym G2. This paper discusses the design and installation of a DeviceNet communication network to smart motor control centers (MCCs) on the three kilns at the Alpena plant. The DeviceNet link, which provides direct digital control and monitoring of motors, is linked to the supervisory system via the remote I/O link.
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DeviceNet在水泥厂电机控制中心的应用
位于密歇根州Alpena的拉法基水泥厂每年从5个窑生产250万吨水泥,每个窑每天生产约1250吨水泥。工厂控制分布在40多个plc5上,有超过18000个I/O点,已经安装了10多年。窑炉是最后的主要设备,但尚未绑定到基于PLC的监控系统。在此基础上选择plc5用于窑炉自动化,并考虑到扩展现有监控系统网络以适应窑炉控制的便利性。工厂架构采用三层通信:第一层,远程I/O从PLC处理器与I/O子系统通信;其次,数据高速公路Plus用于处理器之间和以太网网关/数据服务器之间的通信。该网关向第三层过程监控网络提供过程数据。过程监控网络由运行intelltion dmac的监控工作站和专家系统LUCIE组成,LUCIE是拉法基自己在Gensym G2上运行的应用程序。本文讨论了在Alpena工厂的三个窑的智能电机控制中心(mcs)上设计和安装DeviceNet通信网络。DeviceNet链路通过远程I/O链路连接到监控系统,提供对电机的直接数字控制和监控。
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