Revamping of crude distillation unit for enhancement of processing capacity and LPG extraction through steady state simulation modeling

IF 0.1 Q4 ENGINEERING, CHEMICAL Journal of the Pakistan Institute of Chemical Engineers Pub Date : 2023-01-05 DOI:10.54693/piche.05022
Muhammad Shafiq Khan, Dr. -Ing Naveed Ramzan
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Abstract

The scope of this work covers the debottlenecking of operational constraints for increasing the processing capacity of crude distillation unit and LPG extraction from crude oil. Simulation modeling on Aspen HYSY V7.1 is used for thoroughly investigating and evaluation of retrofit alternatives. Design and operations data of a crude distillation unit at Attock Refinery Limited is used as a case study. Capacity expansion through the addition or rearranging of circulating reflux/Pump-around is selected among the various available revamp alternates like addition of Pre-flash columns, tray geometry and hydraulics etc. Then crude distillation unit is revamped for maximum possible expansion in processing capacity by re-arranging of Pump-around circuits. Pump-around balances re-arranged based on specific crude oil operating blend. Some modifications are also proposed in stabilizer section of the crude distillation unit to enhance LPG extraction from crude oil and finally crude distillation unit simulated for revamped processing capacity with re-arranged pump-around circuits and suggested modifications in stabilizer section. The results of Simulation Modeling validate propose modifications for revamping of processing capacity and LPG extraction.
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通过稳态仿真建模,对原油蒸馏装置进行改造,提高处理能力和液化石油气的提取
这项工作的范围包括消除操作限制的瓶颈,以提高原油蒸馏装置的处理能力和从原油中提取液化石油气。在Aspen hyysy V7.1上进行仿真建模,用于彻底调查和评估改造方案。以阿托克炼油有限公司原油蒸馏装置的设计和运行数据为例进行了研究。通过增加或重新安排循环回流/泵绕流来扩大产能是在各种可用的改造替代方案中选择的,如增加预闪蒸塔、托盘几何形状和液压等。然后对原油蒸馏装置进行改造,通过重新布置绕泵回路,最大限度地扩大处理能力。根据特定的原油操作混合物重新安排泵周围平衡。对原油蒸馏装置稳定器段进行了改造,以提高原油中液化石油气的提取,并最终对原油蒸馏unitÂ进行了模拟,对改造后的处理能力进行了改造,并对稳定器段提出了改造建议。仿真建模的结果验证了对加工能力和液化石油气开采改造的建议。
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