Deploying the World's Largest Bismuth Alloy Plug for Cost Effective P&A

D. Talapatra, P. Carragher
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Abstract

This paper focusses on the successful re-abandonment of a subsea well in the Gulf of Mexico using a rigless approach. The operator had already abandoned the well using conventional technology, but it was still bubbling. The objective was to re-abandon the well by setting a reliable and permanent gas tight seal in the 36" conductor. To achieve this a herculean engineering and operational feat was undertaken to design and manufacture a custom tool using record breaking volume of bismuth and thermite. The tool was deployed from a lift boat and guided into the conductor using ROV's. A timer activation mechanism initiated the thermite heater melting the bismuth alloy cast on to the outside of the tool. The bismuth alloy once molten flowed into the well filling the entire cross section of the 36" conductor. The thermite heater was then retrieved from the molten alloy leaving a solid gas tight metal to metal seal inside the conductor. Observations confirmed the success of the operation, as the bismuth alloy plug created a reliable gas tight seal, with no observed bubbles for a duration of 20 hours. By utilizing bismuth alloy technology, the complexity associated with traditional abandonment methods was eliminated, while ensuring long term reliability. The use of bismuth alloy allowed for a shorter plug length, enabling deployment in the shallow conductor without extensive workover efforts not only reducing costs but also saving time and mitigating HSE risks.
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部署世界上最大的铋合金塞,实现成本效益型 P&A
本文重点介绍了在墨西哥湾采用无钻机方法成功重新废弃一口海底油井的情况。作业者已经使用传统技术弃井,但油井仍在冒泡。目的是通过在 36 英寸导管中设置可靠的永久性气密密封来重新弃井。为实现这一目标,在工程设计和操作方面进行了艰苦卓绝的努力,设计并制造了一种定制工具,使用了创纪录的铋和热石墨。该工具从升降船上部署,并通过遥控潜水器引导进入导体。定时器启动装置启动热敏加热器,熔化铸在工具外部的铋合金。铋合金熔化后流入井中,填满了 36 英寸导体的整个横截面。然后,从熔化的合金中取出热敏加热器,在导体内部留下一个坚固的气密金属密封圈。观察结果证实了这次作业的成功,因为铋合金塞形成了可靠的气密密封,在 20 个小时的持续时间内没有观察到气泡。通过使用铋合金技术,消除了传统废弃方法的复杂性,同时确保了长期可靠性。使用铋合金可以缩短堵塞长度,从而无需大量的修井工作就能在浅层导管中部署堵塞,这不仅降低了成本,还节省了时间,降低了 HSE 风险。
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