Analisis Kinerja Kompressor Screw Oil Injected Sullair Ls20-150h untuk Ash Handling (Study Kasus PLTU Teluk Sirih)

M. Abdillah, Mukhnizar Mukhnizar, Risal Abu, Afdal Afdal, Z. Zulkarnain
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Abstract

PLTU Teluk Sirih is a coal-fired steam power plant as an energy source that produces ash with a capacity of 2 . The compressor is a medium for transferring ash by using compressed air. The compressor used is a SCREEW OIL INJECTED SULLAIR LS20-150H compressor. Currently there is a decrease in performance on the compressor, which initially had a compression ratio of 1,600 Psia, polytropic head 14,500,599, capacity 10,938,438, flow rate 11,379,622 lb/s, efficiency 98.5%. After analyzing this compressor, the data obtained was a compression ratio of 1,540 Psia, polytropic head 13,805,166, capacity 10,950,733, flow rate 11,392,412, and efficiency of 95.3%. The reason is because the compressor room area does not have an active blower so that dirt/ash stuck to the radiator fins causes heat transfer to be hampered and this greatly affects the performance of the compressor parts to work optimally
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用于灰处理的 Sullair Ls20-150h 喷油螺杆式压缩机性能分析(PLTU Teluk Sirih 案例研究)
直落西里(PLTU Teluk Sirih)是一家燃煤蒸汽发电厂,以煤灰为能源,发电量为 2.5 万千瓦时。压缩机是利用压缩空气输送灰烬的介质。使用的压缩机是 SCREEW OIL INJECTED SULLAIR LS20-150H 压缩机。该压缩机最初的压缩比为 1,600 Psia,压头为 14,500,599 个,容量为 10,938,438 个,流量为 11,379,622 磅/秒,效率为 98.5%。对该压缩机进行分析后得出的数据为:压缩比 1,540 Psia,多回转压头 13,805,166,容量 10,950,733,流量 11,392,412,效率 95.3%。原因是压缩机房区域没有主动式鼓风机,因此散热器翅片上粘有污垢/灰尘,导致传热受阻,这极大地影响了压缩机部件的性能,使其无法达到最佳工作状态。
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