{"title":"ANALISIS DAMPAK OVERLOAD TRANSFORMATOR TERHADAP KUALITAS DAYA GARDU K622 PENYULANG PELANGI PT. PLN ( PERSERO ) ULP KARANG","authors":"Jeckson Jeckson, Azis Prayuda, Yenni Afrida","doi":"10.36269/jtr.v4i1.986","DOIUrl":null,"url":null,"abstract":"Transformer overload occurs in one of the distribution transformers in PT. PLN (Persero) ULP Karang,namely the K622 Distribution Transformer at the Rainbow Feeder with a load of 110.16% exceeding the standard set by SPLN, which is 80%. This study aims to find out how to overcome the Overload problem in the K622 distribution substation transformer on The Rainbow and get the size of the K622 distribution substation transformer load before and after the Uprating Transformer. From the results of uprating, the percentage of transformer loading value before uprating transformers was carried out by 110.16% and after uprating transformers by 26.38% so that it decreased by 83.78%. This means that the uprating transformer is one of the methods that can be used to overcome excess loads.","PeriodicalId":31626,"journal":{"name":"Volt Jurnal Ilmiah Pendidikan Teknik Elektro","volume":"8 1","pages":""},"PeriodicalIF":0.0000,"publicationDate":"2022-05-31","publicationTypes":"Journal Article","fieldsOfStudy":null,"isOpenAccess":false,"openAccessPdf":"","citationCount":"0","resultStr":null,"platform":"Semanticscholar","paperid":null,"PeriodicalName":"Volt Jurnal Ilmiah Pendidikan Teknik Elektro","FirstCategoryId":"1085","ListUrlMain":"https://doi.org/10.36269/jtr.v4i1.986","RegionNum":0,"RegionCategory":null,"ArticlePicture":[],"TitleCN":null,"AbstractTextCN":null,"PMCID":null,"EPubDate":"","PubModel":"","JCR":"","JCRName":"","Score":null,"Total":0}
引用次数: 0
Abstract
Transformer overload occurs in one of the distribution transformers in PT. PLN (Persero) ULP Karang,namely the K622 Distribution Transformer at the Rainbow Feeder with a load of 110.16% exceeding the standard set by SPLN, which is 80%. This study aims to find out how to overcome the Overload problem in the K622 distribution substation transformer on The Rainbow and get the size of the K622 distribution substation transformer load before and after the Uprating Transformer. From the results of uprating, the percentage of transformer loading value before uprating transformers was carried out by 110.16% and after uprating transformers by 26.38% so that it decreased by 83.78%. This means that the uprating transformer is one of the methods that can be used to overcome excess loads.
PT. PLN (Persero) ULP Karang的其中一台配电变压器发生变压器过载,即彩虹馈线处的K622配电变压器,其负荷超出SPLN规定的80%的标准110.16%。本研究旨在找出如何克服彩虹号上K622配电变电站变压器的过载问题,得到升级变压器前后K622配电变电站变压器负荷的大小。从升级结果来看,变压器升级前和升级后的负荷值分别占比分别为110.16%和26.38%,降低了83.78%。这意味着升级变压器是可以用来克服过载的方法之一。