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引用次数: 0

摘要

一种用于拉伸预应力混凝土中钢筋的工具失效了。8个个体的下颚都断了。断口表面的目视检查表明,大约一半的断裂部分具有部分树枝状外观。此外,零件外部附近的断口表面干净光滑,有病例的证据。对零件平面的检查发现,在实际故障没有发生的地方,表面出现了裂纹。化学分析表明该材料为低合金渗碳钢。该组织与铸钢、渗碳、淬火、回火相适应。结构总体上是令人满意的,除了存在严重的收缩孔隙。结论认为,关键区域的收缩孔隙是导致断裂的主要原因。极高的硬度表明缺乏适当的回火是次要原因。
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Failure of Steel Jaws
A tool used to stretch reinforcement wires in prestressed concrete failed. All eight individual jaws were broken. Visual examination of the fracture surfaces indicated that about half of the broken parts had a partially dendritic appearance. Further, fracture surfaces near the exteriors of the parts were clean and smooth, and there was evidence of a case. Examination of the flat surfaces of the parts revealed surface cracking where actual failure had not occurred. Chemical analysis showed the material to be a low-alloy carburizing steel. The microstructure was compatible with a steel which is cast, carburized, quenched, and tempered. The structure was generally satisfactory, except for the presence of severe shrinkage porosity. It was concluded that the presence of shrinkage porosity in critical areas was the primary cause of fracture. Extremely high hardness indicating a lack of adequate tempering was the secondary cause.
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