现有原型机械脱石机的改造和性能评估

Koyenikan, O.O., Filani, A.O.
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摘要

为了提高效率,对现有的机械式大米去石机进行了改造。我们发现,现有机器的性能存在一些问题,使其无法有效工作。为了改造现有的机械式碎米机,我们采用了弹簧、缓冲橡胶、线圈、电容器、电缆和插头。机器改装后,进行了性能评估。总共 6 公斤脱粒大米样品与 2.36 毫米大小的石头混合,分成 1.5 公斤、2.0 公斤和 2.5 公斤三部分,分别标为 A、B 和 C。每一部分在不同时间被送入大米脱石机中进行脱石。此外,还取 200 克脱粒后的大米进行人工挑拣,作为分离大米中其他异物的对照。这是用来比较机器效率的结果。经测定,手捡法的效率为 80%,而改良脱石机的效率分别为 66.7%、60% 和 64%。因此,机械式大米去石机的性能评价高于平均水平,但不如手选法有效。此外,当进料量为 1.5 千克、2.0 千克和 2.5 千克时,机器的吞吐能力分别为 13.60 千克/小时、15.38 千克/小时和 15.38 千克/小时。因此,改进后的机械式大米去石机将被用作建造其他新型大米去石机的模板。
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Modification and Performance Evaluation of an Existing Prototype Mechanical Rice De-stoner
An existing mechanical rice de-stoner was modified for the purpose of improving its efficiency. Some challenges were discovered with the performance of the existing machine that did not make it to perform effectively. The spring, cushion rubber, coil, capacitor, cable and plug were incorporated to modify the existing mechanical rice de-stoner. After modification of the machine, performance evaluation was carried out. A total of 6 kg of threshed rice sample was mixed with stones sized 2.36mm and was divided into three parts of 1.5kg, 2.0kg and 2.5kg and labelled A, B and C respectively. Each part was fed at different times into the rice de-stoner and de-stoned. Also, 200g of the threshed rice were taken for hand-picked which served as the control for separating and other foreign materials from the rice. This was used to compare the result of the efficiency of the machine. The efficiency of the handpicked method was determined to be 80% while that of the modified de-stoner was determined to be  66.7%, 60% and 64% respectively. Thus the performance evaluation of the mechanical rice de-stoner was rated above average but not as effective as the hand-picked method. Also, the machine`s throughput capacity was 13.60 kg/hr, 15.38 kg/hr and 15.38 kg/hr for the feed rates of 1.5kg, 2.0kg and 2.5kg respectively.. Thus, the modified mechanical rice de-stoner machine was to be used as a template for other new rice de-stoner to be constructed.
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