Noise Logging Application for Well Integrity Evaluation: A Case Study in Peninsular Malaysia

L. J. Saw, Hanalim Linda, Tolioe Amelio William
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Abstract

Field-X was first discovered in 1979, comprising of saturated oil reservoirs with several shallower non-associated gas reservoirs. Field-X is currently producing from several oil producers. X8 well was recently drilled, completed, and produce from A and B reservoirs. However, 5 months later, the oil rate has been reduced by half with gas oil ratio (GOR) increased up to 5 times. Consequently, the well had to be shut-in due to reservoir management plan (RMP) violation. X9 well was drilled and completed, but 5 years later the well started experiencing the sustained production casing pressure (PCP) and was forced to shut-in in the following year with the locked-in potential of both A and B reservoirs. To diagnose the root cause of high GOR (HGOR) in X8 well and sustained PCP in X9 well, the Spectral Noise Log (SNL) was deployed. The main advantage of utilizing SNL is its capability of detecting fluid movement behind tubing and casing. High differential pressure creates lots of fluid movement, which generates higher noise amplitude. Meanwhile, smaller pores or leaks generate higher frequency noise that can be easily picked up by SNL. SNL tool was run in flowing condition for X8 well and the results indicated the HGOR zones were mainly contributed by the shallower B05 sand which was flowing through the leaked 4-1/2″ liner packer. Temperature deflections also indicated that the liner packer seal was leaking and B05 reservoir was contributing to the production. The liner packer leak and B05 reservoir flow would not have been detected by conventional production logging tools as the flow was happening beyond the tubing and casing. For X9 well, SNL was run in the wellbore whilst pumping water via annulus, through the leaks and flowing back up the tubing. Three tubing leaks were successfully detected from the SNL run, whereas previous conventional noise log only managed to detect 2 leaks. It is possible that the third small leak was very small, hence the conventional tool was unable to detect it. X8 well successfully back online with 8.4% rate increase than last production with GOR reduced back to initial GOR and X9 well successfully back online as per last production rate. The liner packers which are not permanent barriers for reservoir isolation and allocation can be validated, moreover, verifying that tubing leakage is mainly contributed by tubing joints, which can be used as the main input in tubing materials selection in the future. Well integrity issues can cause significant loss of production, oil spill or worst case, even loss of lives. Proper selection in data acquisition tools helps to accurately diagnose well integrity issues that can be swiftly addressed. In the low oil price environment, skimming down on data acquisition costs may not uncover the true underlying well issues or reservoir issues, but might jeopardize future projects to be undertaken in years to come.
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噪声测井在井完整性评价中的应用:以马来西亚半岛为例
x油田于1979年首次被发现,包括饱和油藏和几个浅层非伴生气藏。Field-X目前正在与几家石油生产商合作。X8井最近在A和B储层钻完井并开始生产。然而,5个月后,出油率降低了一半,气油比(GOR)提高了5倍。因此,由于违反了油藏管理计划(RMP),该井不得不关井。X9井已经钻完井,但5年后,该井开始出现持续的生产套管压力(PCP),并在第二年被迫关闭,A和B储层都具有锁定潜力。为了诊断X8井高GOR (HGOR)和X9井持续PCP的根本原因,使用了频谱噪声测井(SNL)。利用SNL的主要优点是能够检测油管和套管后面的流体运动。高压差造成大量流体运动,产生较大的噪声幅值。同时,较小的孔隙或泄漏会产生更高频率的噪声,这些噪声很容易被SNL拾取。在X8井的流动状态下下入SNL工具,结果表明,HGOR层主要是由流过泄漏的4-1/2″尾管封隔器的浅层B05砂造成的。温度偏差也表明尾管封隔器密封泄漏,B05储层影响了产量。常规的生产测井工具无法检测到尾管封隔器泄漏和B05油藏流动,因为流动发生在油管和套管之外。对于X9井,SNL在井筒中下入,同时将水通过环空泵入,穿过泄漏并沿油管回流。SNL下入成功检测到3处油管泄漏,而之前的常规噪声测井只能检测到2处泄漏。有可能第三个小泄漏非常小,因此常规工具无法检测到它。X8井成功恢复生产,产量比上次增加8.4%,GOR降至初始GOR, X9井按上次产量成功恢复生产。验证了尾管封隔器不是油藏隔离和配置的永久屏障,验证了油管泄漏主要是由油管接头造成的,这可以作为今后油管材料选择的主要依据。油井完整性问题可能会造成重大的生产损失、石油泄漏,甚至在最坏的情况下,造成人员伤亡。正确选择数据采集工具有助于准确诊断井的完整性问题,并迅速解决问题。在低油价环境下,降低数据采集成本可能无法发现真正潜在的井或油藏问题,但可能会危及未来几年的项目。
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