采用铜柱凸点作为第一次互连的45纳米极低k芯片的挑战

Po-Jen Cheng, C. Chung, T. Pai, D. Y. Chen
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引用次数: 13

摘要

本研究首次在65 nm低k芯片的FCCSP上构建了铜柱凸点。设计了7个DOE电池,评估了铜柱高度、铜柱直径、PI开口尺寸和PI材料对封装可靠性性能的影响。经过封装组装和长期可靠性试验,未发现明显故障。虽然可靠性测试时间延长至原来的3倍,但封装仍然保持良好状态。在65纳米低k芯片上的铜柱凸点的经验基础上,采用45纳米ELK芯片的FCBGA封装再次构建了铜柱凸点。通过CSAM检测发现贴片粘结后出现白色凸起缺陷,失效分析表明白色凸起现象是由于ELK层内部出现裂纹所致。采用局部加热粘结工具(热压粘结)对ELK裂纹进行了改善,试验结果表明ELK裂纹仍然存在,但故障率由原来的30%~50%降低到5%~20%。模拟分析了PI开孔尺寸和UBM尺寸对ELK层应力集中的影响。较小的PI开口尺寸可以减小ELK层的应力分布。相反,较大的PI开孔尺寸和较大的UBM尺寸对ELK裂纹也有积极的影响。再次进行了装配工艺和可靠性试验,验证了仿真结果,实验数据与仿真结果一致。
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A challenge of 45 nm extreme low-k chip using Cu pillar bump as 1st interconnection
In this study, Cu pillar bump is firstly built on FCCSP with 65 nm low k chip. 7 DOE cells are designed to evaluate the effects of Cu pillar height, Cu pillar diameter, PI opening size and PI material on package reliability performance. No obvious failure is found after package assembly and long-term reliability test. The packages are still in good shape even though the reliability test is expanded to 3x test durations With the experiences of Cu pillar bump on 65 nm low k chip, Cu pillar bump is again built on FCBGA package with 45 nm ELK chip. White bump defect is found after chip bond via CSAM inspection, failure analysis shows that the white bump phenomenon is due to crack occurs inside ELK layer. A local heating bond tool (thermal compression bond) is used to improve ELK crack, test results illustrate ELK crack still exists, however the failure rate reduces from original 30%~50% to 5%~20%. Simulation analysis is conducted to study the effect of PI opening size and UBM size on stress concentration at ELK layer. Small PI opening size can reduce stress distribution at ELK layer. On the contrary, relatively large PI opening size and large UBM size also show positive effect on ELK crack. Assembly process and reliability test are conducted again to validate simulation results, experiment data is consistent with simulation result.
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