利用永久光纤分布式温度传感技术对马来西亚海上B油田气举生产商进行增产评估

Chang Siong Ting, N. Minggu, Dahlila Kamat, Kit Teng Chaw, Chee Seong Tan, Sanggeetha Kalidas, Gladson Joe Barretto
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引用次数: 0

摘要

在本文中,我们利用分布式温度传感(DTS)技术评估了B井长管柱(即BL井)增产活动的有效性。在整个储层段安装永久性光纤电缆,可以进行气举监测,识别井的完整性问题,并根据射孔贡献进行层间流入剖面分析。最近的DTS解释表明,由于气举不理想,泄漏点在4025英尺处,造成300桶/天的损失。因此,连续进行了油管修补和气举阀更换(GLVC)等修井作业,以恢复其初始产量。所执行的补救工作的有效性将与DTS的温度测量结果和解释一起讨论。BL井是一个长管柱气举生产商,从两个区域流出。在进行油管修补之前,将多指测径器工具登录到BL井,进一步验证DTS指示的泄漏点。井径测井测量发现,最大穿透深度(100%)发生在4025英尺处,这将其归类为泄漏孔。特别是延时DTS测量;获取油管前、油管中、油管后贴片和GLVC。与永久井下压力表(PDG)数据和地面参数(如油管头压力(THP)、套管头压力(CHP)、气举注入速率等)一起进行分析。多测量解释进一步补充节点分析更结论性的发现。在关井期间获得基线温度,作为地热梯度参考,以确定每次事件期间获得的温度是否存在异常。作业快速查看表明,GLVC和油管补丁都被认为是成功实施的,修井挑战最小。然而,执行的补救工作预计将从BL井恢复到最初的生产,但结果表明,该井的表现仍然不佳。作业后执行过程中,生产速率持续下降。DTS温度曲线的定性解释显示,在油管修补后4007英尺处检测到另一个明显的油管泄漏。偶然发现,DTS数据还显示,顶部层(短管柱)的产量是通过长管柱的泄漏孔生产到地面的。通过节点分析和PDG数据的进一步研究表明,在长管柱处,观察到从顶部生产层穿过底部泄漏孔的横向流动。这导致了BL井严重的产量损失。此外,温度分布表明,由于多指向,注入的气体无法到达孔口(操作节点),从而导致该井在补救作业后的生产表现不佳。在本研究中,DTS数据为BL井实施的补救工作的有效性提供了有价值的发现。DTS测量和监测被证明是有用的,是一种创新的替代方案,可以决定任何改善石油的补救工作是否成功,而不是记录在纸上的“完美执行”。
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Production Enhancement Evaluation via Permanent Fiber Optics Distributed Temperature Sensing Interpretation for a Gas-Lifted Producer in Field B, Offshore Malaysia
In this paper, we evaluate the effectiveness of production enhancement activities for well B Long-string (i.e. well BL) using distributed temperature sensing (DTS) technology. Installation of permanent fiber-optic cable across the reservoir sections has enabled gas lift monitoring, identification of well integrity issues and zonal inflow profiling from perforation contribution. Recent DTS interpretation indicated leak point at 4,025ft with sub-optimal gas lifting which has resulted in loss of 300 BOPD. Hence, well intervention such as tubing patch and gas lift valve change-out (GLVC) were conducted consecutively to restore its initial production. The effectiveness of executed remedial jobs will be discussed along the findings and interpretations of the temperature survey result from DTS. Well BL is a long-string gas lifted producer that flows from two zones. Prior to the tubing patch, the multi-finger caliper tool was logged in well BL to further validate the leak point indicated by DTS. The caliper logging survey identified that maximum penetration (100%) occurs at 4,025 ft, which classified it as a leak hole. Time-lapsed DTS measurement, specifically; pre-, during-, and post-tubing patch and GLVC were acquired. It is analyzed along with Permanent Downhole Gauge (PDG) data and surface parameters [e.g., tubing head pressure (THP), casing head pressure (CHP), Gas lift injection rate, etc]. The multi-measurement interpretation is further complemented by nodal analysis for a more conclusive finding. A baseline temperature was acquired during the shut-in period as a geothermal gradient reference to determine any anomalies against the temperature acquired during each event. Operation quick-look indicated both GLVC and tubing patch are deemed to be successfully carried out as per the program with minimal workover challenges. However, the executed remedial jobs that are expected to resume the production from Well BL to its initial production shows it is still underperforming. Production rate keeps declining during the post-job execution. Qualitative interpretation from DTS temperature profiles, reveals another significant tubing leak detected at 4,007ft after the tubing patch. By accidental find, the DTS data also showed that the production from top zone (short string) was produced through the leak hole at the long string to surface. Further investigation applying nodal analysis and PDG data indicated that crossflow was observed from the top zone production through and into bottom leak hole at the long string. This has led to serious production loss in well BL. Furthermore, temperature profile that's demonstrated the injected gas was unable to reach the orifice (operating node) due to multi-pointing, thus resulted in the well's underperforming production post-remedial job execution. In this root-cause finding showcase, DTS data have been providing valuable findings on the effectiveness of executed remedial jobs in well BL. DTS measurement and monitoring is proven useful and as an innovative alternative for deciding the definite success of any remedial job to improve oil, against the recorded "flawless execution" on paper.
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