First Implementation of Managed Pressure Drilling (MPD) System in Swamp Barge Rig to Drill Narrow Pressure Window HPHT Exploration Well Safely – Return of Experience from Kalimantan, Indonesia

_. Setiohadi, Praja Hadistira, Muhammad Alfianoor Yudhatama, Daniel Sitompul, Dikha Escodianto Hutabarat, Andre Wiharja, C. Agriawan, A. Martadinata, _. Sudiariaji, Agus Sidianto, Andry Prasthio, F. Irawan
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Abstract

The first ever HPHT exploration well in Kalimantan was drilled by Swamp Barge Rig with narrow pressure window environment. The well was planned to be drilled using 2.9 SG mud weight to 4575 m vertical depth with 0.10 SG pressure window. Maximum predicted bottom hole temperature of the well was 186° C while the maximum expected wellhead pressure (MEWHP) reached 11,300 Psi. MPD becomes mandatory to complete the well and becomes a novel implement for swamp barge rig operation. Therefore, MPD workshop was held among the teams to ensure all personnel become familiar with the system. On other hand, the equipment configuration was set with some modifications to accommodate the operation requirement, contingency, tight stack up below rotary table and hoisting devices limitation. Rotating Control Device (RCD) was stacked up part by part on tight moon pool space. Several modifications were done properly and gave operation flexibility plus robust contingency. RCD alignment was reset periodically and natural rubbers were utilized to enhanced rubbers lifetime in high temperature condition. EKD system with Coriolis utilization was being main mitigation during drilling with limited kick margin that will allow reservoir section to be accessed. Formation pressure investigation was also performed to give additional information on formation pressure for better well assessment. SBP application on dual gradient tripping and managed pressure cementing give a means to secure the well safely and properly during high gas event with losses condition. As the result, MPD implementation enables the operator to complete HPHT exploration well on swamp barge rig project safely despite the complexity and risk of narrow formation pressure window operation.
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首次在沼泽驳船钻井平台上实施控压钻井(MPD)系统,安全钻出窄压力窗高温高压探井——印度尼西亚加里曼丹经验的回馈
加里曼丹第一口高温高压探井是用窄压力窗环境下的Swamp Barge钻机钻探的。该井计划使用2.9 SG泥浆密度,井深4575米,压力窗0.10 SG。该井的最大预测井底温度为186℃,最大预期井口压力(MEWHP)达到11,300 Psi。MPD已成为完井作业的必备工具,并成为沼泽驳船钻井作业的新工具。因此,在各小组之间举行了MPD讲习班,以确保所有人员熟悉该系统。另一方面,设备配置进行了一些修改,以适应作业要求、应急情况、转盘以下紧密堆叠以及吊装设备的限制。旋转控制装置(RCD)在狭小的月池空间上逐块堆放。通过适当的修改,提高了操作的灵活性和鲁棒性。定期重置RCD对准,并利用天然橡胶提高橡胶在高温条件下的使用寿命。在有限的井涌余量下,利用科里奥利的EKD系统是钻井期间的主要缓解措施,这将允许进入储层段。此外,还进行了地层压力调查,以获得更多的地层压力信息,从而更好地进行井评价。SBP在双梯度起下钻和控压固井中的应用,为在高含气量、漏失情况下安全、合理地保护油井提供了一种手段。因此,MPD的实施使作业者能够安全完成沼泽驳船钻井项目的高温高压探井,尽管地层压力窗口操作的复杂性和风险很小。
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