Achieving stretched capacity goal through integrated engineering and manufacturing excellence

R.S.T. Kwooi
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Abstract

Achieving stretched equipment capacity and high productivity in high volume manufacturing is a gritty challenge to drive down cost continuously in this competitive chipset market. With unprecedented volume ramp of both key products in Q4'99, the Test Module faced a shortage of two to four testers. Driving through working group, a refurbishment process was achieved successfully resulting in 60% reduction of tester faults thus improving mean time between failure (MTBF) from 140 hrs to 160 hrs. With the implementation of improved pogo pins at Tester Interface Unit (TIU) and test head had improved cleaning frequency from 5 k to 90 k, one-sum test yield from 88.7% to 97.5% and reduced non-genuine SBL from 10% to less than 3% consistently.
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通过集成工程和卓越制造实现产能目标
在这个竞争激烈的芯片组市场上,在大批量生产中实现设备产能和高生产率是一项艰巨的挑战。随着99年第四季度这两款关键产品的空前产量增长,测试模块面临着两到四名测试人员的短缺。在工作组的推动下,一个翻新过程成功实现,使测试仪故障减少了60%,从而将平均故障间隔时间(MTBF)从140小时提高到160小时。在测试接口单元(TIU)和测试头安装改进的弹簧销后,清洗频率从5k提高到90k,一次性测试收率从88.7%提高到97.5%,并将非正品SBL从10%降低到3%以下。
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