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Increase the Effectiveness of Water Shutoff Operation Using Acoustic Leak Detection and Pressure Thermal Log in Mature Field South Sumatera – Indonesia 利用声波检漏和压力热测井技术提高印尼南苏门答腊成熟油田堵水作业的有效性
Pub Date : 2023-03-14 DOI: 10.2118/212934-ms
Nayung Galih Proboseno, Aris Nur Atmiaji, A. Suryana, Rudhy Setiawan, Adhyasa Humam Haryaputra, Taufik Fansuri, Masrul Ali Jusda
The evaluation of flow profile in the wellbore system is an important part of oil & gas field development. Leaks that occur in or behind the production casing is not only potentially causes safety and environmental issue but also potentially misjudgments of production performance analysis and the estimation of remaining reserve. The flow profile in the wellbore mostly affected by the life cycle of well during drilling phase, completion phase, production or injection phase and restoration phase. One of many well-known technologies applied in oil & gas industries is acoustic leak detection and pressure thermal log. The selection of surveillance technique to identify undesired water flow problem is not only provides more effective result but also carries an acceptable risk in term of the project cost. The objective of this paper is to show how a new approach of acoustic leak detection and pressure thermal surveillance can be used to increase the effectiveness of water shutoff operation in mature oil and gas field. The new approach of dynamic surveillance technique provided the acoustic, pressure and thermal data acquisition along the artificial lift wells can be interpreted. The case studies shows that the undesired water flow in or behind production casing can be identified precisely compared with a conventional method such as cement bond log. As the result, the data interpretation gives a remarkable result both of the successful water shutoff operation and post job production performance. Water significantly can be reduced from 1300 bbl per day to 320 bbl per day and the other hand oil & gas significantly can be increased from 34 boepd to 532 boepd. Moreover, this paper should be beneficial to help all petroleum engineers currently working in mature oilfield not only to identify undesired water flow problem precisely but also develop a comprehensive and effective water shutoff and remediation plan.
井筒系统流动剖面评价是油气田开发的重要组成部分。发生在生产套管内部或背后的泄漏,不仅可能造成安全与环境问题,而且可能导致生产动态分析和剩余储量估计的错误判断。在钻井阶段、完井阶段、生产或注入阶段和恢复阶段,井内流动剖面主要受井生命周期的影响。声学泄漏检测和压力热测井是油气行业中应用最为广泛的技术之一。监测技术的选择不仅能提供更有效的结果,而且在工程成本方面具有可接受的风险。本文的目的是展示如何利用声波泄漏检测和压力热监测的新方法来提高成熟油气田堵水作业的有效性。动态监测技术的新方法为人工举升井沿线的声、压、热数据采集提供了解释。实例研究表明,与水泥胶结测井等常规方法相比,可以精确识别生产套管内或背后的不良水流。因此,数据解释在成功的堵水作业和作业后的生产性能方面都取得了显著的成果。水可以从1300桶/天显著减少到320桶/天,另一方面,油气可以从34桶/天显著增加到532桶/天。对于目前在成熟油田工作的石油工程师来说,不仅能准确识别出不希望出现的水流问题,还能制定出全面有效的堵水修复方案。
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引用次数: 0
Complex Operation to Insert Coiled Tubing Through Parted Production Tubing and Regain Pressure Integrity for Plugging and Abandonment 通过分离的生产油管插入连续油管并恢复封堵和弃井的压力完整性的复杂操作
Pub Date : 2023-03-14 DOI: 10.2118/212879-ms
Sergio A Rondon Fajardo, E. Adams
At the end of 2020, complex well anomalies were identified in the previously shut-in, highly deviated well A in deepwater Gulf of Mexico. Closely monitored wellbore pressures indicated A/B annulus communication, and remedial slickline diagnostics discovered the tubing was parted between ~4,250 and 4,270 ft measured depth. The abnormal well conditions and the presence of a single barrier on both the A-annulus and B-annulus triggered the well anomaly process, and action was taken to mitigate the risk profile by commencing abandonment operations prior to the start of the hurricane season. The well anomaly risk assessment indicated the highest risk was the single barrier on the B-annulus as it had a history of failures and repairs. The outcome was to attempt to further mitigate the risk profile by commencing zonal isolation operations. To achieve a safe operation, a real-time coiled tubing (CT) downhole measurement system and dynamic interpretation software were used to mitigate the risks involved in accessing the lower section of the parted production tubing, pressure testing the completion, perforating the tubing, confirming the firing of the tubing-conveyed perforating guns, and pumping a balanced cement plug in the tubing and annulus after setting the cement retainer. This study proposes an innovative approach to integrating CT, telemetry, and mechanical wellbore isolation tools to increase operational efficiency. Real-time bottomhole pressure, temperature, and casing collar locator (CCL) measurements proved invaluable by providing the necessary guidance to successfully set the inflatable packer and fire the perforating guns. They also provided pressure confirmation that tubing integrity issues did not allow cement in the A-annulus to escape into the production tubing on to the backside of the CT.
2020年底,在墨西哥湾深水区先前关闭的大斜度井A中发现了复杂的异常井。密切监测的井筒压力表明A/B环空连通,修复钢丝绳诊断发现油管在测量深度~ 4250 ~ 4270英尺之间分离。异常的井况以及a环空和b环空存在的单一屏障触发了井的异常过程,为了降低风险,公司采取了措施,在飓风季节开始之前开始了弃井作业。井异常风险评估表明,风险最高的是b环空的单个屏障,因为它有故障和维修的历史。结果是试图通过开始层间隔离作业来进一步降低风险。为了实现安全作业,作业人员使用了实时连续油管(CT)井下测量系统和动态解释软件,以降低进入分离生产油管下部、完井压力测试、射孔油管、确认射孔枪发射、在水泥保持器坐封后向油管和环空泵入平衡水泥塞等过程中的风险。该研究提出了一种整合CT、遥测和机械井眼隔离工具的创新方法,以提高作业效率。事实证明,实时井底压力、温度和套管接箍定位器(CCL)的测量非常宝贵,为成功坐封膨胀封隔器和射孔枪提供了必要的指导。他们还提供了压力确认,油管完整性问题不允许a环空的水泥逃逸到连续油管后部的生产油管中。
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引用次数: 0
Thru Tubing Inflatable Retrievable Bridge Plug Deployed on Coiled Tubing in Low Pressure Gas Wells with ID Restrictions for Workover Operations - A Case History from China 在具有内径限制的低压气井修井作业中,连续油管上可伸缩桥塞应用于连续油管上——中国案例
Pub Date : 2023-03-14 DOI: 10.2118/212901-ms
Lei Hou, Chong Zhang, Xin Zhi Hou, Yong Jia Dong, Yu Zhao Peng, Vaibhav Gupta, V. Unnikrishnan, Feng Li Wei, Lin Guo Li, Feng Yi Wu, Yang Ming Huang, Zhen Hua, Lin Hou Li
A workover campaign in low bottomhole pressure gas wells in China South Sea was planned, where a through tubing retrievable inflatable bridge plug (TTIRBP) was chosen to provide zonal isolation. Challenging circumstances include zero fluid contamination allowed, small through tubing restriction as opposed to large setting ID, shallow working depth and tight working schedule to complete the workover activity during the typhoon season. To mitigate the fluid contamination challenge, Nitrogen-driven setting of TTIRBP was selected. Through Tubing Intervention (TTI) services were safely and successfully completed by nitrogen-driven in all six wells via coiled tubing deployment and met the customer workover schedule deadline. After that, these gas wells were recovered to the same initial production rate quickly and efficiently. This paper will provide operational details for the 6 wells in this campaign. These methods are described in detail to share the valuable experience for readers’ similar application.
该公司计划在中国南海的低井底压力气井中进行修井作业,选择了一种可通过油管回收的膨胀桥塞(TTIRBP)来进行层间隔离。具有挑战性的环境包括零流体污染、小的过油管限制(而不是大的坐封内径)、浅的工作深度以及在台风季节完成修井作业的紧凑工作计划。为了减轻流体污染的挑战,选择了氮驱动的TTIRBP设置。通过油管修井(TTI)服务通过连续油管下入氮气驱动,安全成功地完成了所有6口井,并满足了客户的修井计划截止日期。之后,这些气井迅速有效地恢复到相同的初始产量。本文将提供该活动中6口井的操作细节。对这些方法进行了详细的描述,为读者的类似应用提供了宝贵的经验。
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引用次数: 1
Eliminating Bradenhead Pressure Using Novel Biomineralization Technology 利用新型生物矿化技术消除布雷登黑德压力
Pub Date : 2023-03-14 DOI: 10.2118/212893-ms
Dwight Randy Hiebert, J. Griffin
An oil well in Colorado had bradenhead pressure of 700 psi on the 9-5/8 in × 5-1/2 in annulus, prompting remediation to get bradenhead pressure below the 200-psi threshold set by the Colorado Oil and Gas Conservation Commission (COGCC) to resume production. A biomineralization company was contracted by an operator in Colorado to apply their proprietary biomineralization technology to the well. Cement bond logs were used to identify a micro annulus around 3,050 ft. The well was prepared by setting a bridge plug at 3,062 ft, perforating at 3,056 ft and 3,052 ft, and running tubing to the depth of the bottom perforation. Biomineralizing fluids were then pumped into the well, where they formed crystalline calcium carbonate in the micro annuli. After 36 hours of treatment, the injection rate dropped by several orders of magnitude. Subsequent monitoring by a state regulator determined bradenhead pressure had been eliminated and the well passed a mechanical integrity test without any additional intervention, allowing production to promptly resume.
科罗拉多州的一口油井在9-5/8英寸× 5-1/2英寸环空的布雷登黑德压力为700 psi,需要进行补救,使布雷登黑德压力低于科罗拉多州油气保护委员会(COGCC)设定的200 psi阈值,才能恢复生产。科罗拉多州的一家运营商与一家生物矿化公司签约,将其专有的生物矿化技术应用于该井。水泥胶结测井用于识别3050英尺左右的微环空。该井的准备工作是在3062英尺处设置桥塞,在3056英尺和3052英尺处射孔,并将油管下至底部射孔深度。然后将生物矿化流体泵入井中,在微环空中形成结晶碳酸钙。治疗36小时后,注射速率下降了几个数量级。随后,国家监管机构进行了监测,确定bradenhead压力已经消除,并且在没有任何额外干预的情况下通过了机械完整性测试,可以立即恢复生产。
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引用次数: 0
Efficient and Reliable Multilateral Coiled Tubing Intervention Technique for Acid Stimulation: A Case History in the Middle East 高效可靠的多边连续油管酸增产干预技术:中东地区的一个历史案例
Pub Date : 2023-03-14 DOI: 10.2118/212921-ms
Hassan Basim Alnasser, Ugochukwu Maria Okeke, Zhiheng Zhang, Ron van der Veen, S. Chishti, S. Umirshin
In recent years, multilateral wells have become more predominant enabling either improved recovery or injectivity depending on the well type. The process of timely accessing the correct lateral with coiled tubing (CT) is still one of the greatest challenges relative to the well intervention. This paper presents a case history in which a flawless 2.375-in CT intervention was performed to stimulate laterals with a proprietary multilateral entry bottom hole assembly (BHA) that steered the CT efficiently into the laterals. The injector well has a natural and un-natural lateral, both of which required stimulation. A proprietary hydraulic multilateral entry tool was selected for the job which reliably locates and enters multiple lateral junctions in a single run. The special working mechanism of the tool circumvents any need for an electrical control or steering system. Along with this tool, a casing collar locator (CCL) was incorporated into the BHA, powered by a proprietary CT conductor telemetry system. Real time data enabled confirmation relative to access into the correct lateral to save time without the need to tag the bottom. A gamma ray (GR) sub can also be incorporated into the BHA to correlate depth where needed. A major challenge for multilateral intervention is time on location. The multilateral entry tool searches for the lateral by rotating 360° until it reaches the desired kick off angle which is confirmed by a surface pressure indication signifying that the correct lateral has been located. The simple yet effective operational mechanism of the multilateral tool allows each lateral to be found and entered in less than 30 minutes once it is positioned at the window. Depth correlation is confirmed with use of either the CCL or GR subs or a combination of the two and the multilateral entry tool is resettable easily by pressurizing, which enables any number of laterals to be located & stimulated. The job was completed safely as per program with more than 4,000 bbl of acid pumped to stimulate both the laterals. The entire operation was conducted efficiently, flawlessly, and post injectivity results of the stimulation resulted in significant incremental injection drainage capability. This combination of BHA's options and the efficient mechanism of the multilateral entry tool to find and enter multiple laterals quickly and reset without the need to pull out of hole, enables the Operator to intervene in any number of branches of a multilateral well in a timely and efficient manner. This is a very important case history for other complex multilateral wells in the region which could benefit from this technology and approach
近年来,多分支井越来越占主导地位,根据井类型的不同,可以提高采收率或注入能力。在修井作业中,利用连续油管(CT)及时进入正确的水平段仍然是最大的挑战之一。本文介绍了一个使用专有的多通道钻具组合(BHA)进行2.375英寸连续油管修井作业的案例,该修井作业能够有效地将连续油管导向分支井。注入井有自然和非自然分支,两者都需要增产。该作业选择了一种专有的液压多分支钻进工具,该工具可以在一次入井中可靠地定位和进入多个分支接头。该工具的特殊工作机构避免了对电气控制或转向系统的任何需要。与该工具一起,套管接箍定位器(CCL)被集成到BHA中,由专有的CT导体遥测系统提供动力。实时数据可以在不需要标记底部的情况下,相对于进入正确的水平段进行确认,从而节省时间。伽马射线(GR)短节也可以集成到BHA中,以便在需要时关联深度。多边干预的一个主要挑战是地点的时间。侧向钻进工具通过旋转360°来搜索分支井,直到达到所需的起斜角度,地面压力指示表明已经定位了正确的分支井。多边工具的操作机制简单而有效,一旦定位到窗口处,就可以在不到30分钟的时间内找到并进入每个分支。通过使用CCL或GR短节或两者的组合,可以确认深度相关性,并且可以通过加压轻松复位多边进入工具,从而可以定位和增产任意数量的分支。作业按照计划安全完成,共泵入了4000桶以上的酸液,对两个分支进行了增产。整个作业进行得非常高效、完美,注入后的增产效果显著提高了注入排水能力。BHA的可选方案与高效的分支进入工具机制相结合,可以快速找到并进入多个分支,无需出井即可进行复位,使作业者能够及时有效地干预分支井的任何分支。对于该地区其他复杂的多边井来说,这是一个非常重要的历史案例,这些井可以从该技术和方法中受益
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引用次数: 0
Production and Well Access Restored After a Successful Subsurface Safety Valve Flowtube Milling on E-line, Preventing Major Rig Workover 井下安全阀流管在e -管线上磨铣成功后,恢复了生产和油井通道,避免了大规模的钻机修井
Pub Date : 2023-03-14 DOI: 10.2118/212884-ms
Juan Jose Nobile Blanco, S. Prabhakaran, Shiwanshu Shiwan, Chirag Rathod, David Ting
An offshore production well was out of operation after unsuccessful inflow tests. A remedial work plan was designed, but the execution resulted in severe damage to the top of the flowtube inside the Subsurface Safety Valve (SSSV), which was bent over and preventing production. Wireline conveyed mechanical intervention was performed with robotic tools to mill the obstruction and regain full bore access. Downhole hardware milling is a common technology; however, a thorough process must be followed in order to succeed. The following factors were among those to be considered: well configuration (completion schematic and restrictions); the material of the flowtube (9CR-1MO Martensitic Steel); the risk of damaging the surrounding area; the risk of rotating the whole assembly while milling; and the risk of getting stuck with the e-line Bottom Hole Assembly (BHA). The milling intervention program was drafted taking into consideration different scenarios including contingencies. E-line conveyed robotic milling intervention was the preferred option due to the urgency of the operation and high accuracy required to ensure the SSSV was left operational after milling. The robotic toolstring was first deployed for a drift run. Subsequent diagnostic runs were executed to help the team understand the downhole situation, adjust the operation plan and to test the performance of the tool downhole. Finally, the milling run was conducted showing a clear signature on the acquisition system, providing the parties involved with certainty regarding the outcome. A camera run was performed to verify the conditions of the operational area after milling. The job was executed in a total of four runs as per the program. Furthermore, the milling time itself was only 17 minutes. The complete removal of the damaged section of flowtube allowed the client to restore production immediately after testing the well integrity, with the SSSV fully functional. This paper describes the complex yet efficient operation where a robotic milling tool, conveyed by e-line, was able to remove a critical downhole obstruction and restore production while preserving all safety features of the well, thus preventing a complex workover operation. The in-depth preparation, followed by a methodical execution, allowed oil production to be resumed in this well.
在流入测试失败后,一口海上生产井停止了作业。设计了补救工作计划,但执行过程中导致地下安全阀(SSSV)内流管顶部严重损坏,导致弯曲,无法生产。利用机器人工具进行电缆输送机械修井作业,磨铣堵塞物,恢复全井眼通道。井下硬件磨铣是一种常见的技术;然而,为了成功,必须遵循一个彻底的过程。需要考虑的因素包括:井的结构(完井示意图和限制条件);流管材质为9CR-1MO马氏体钢;破坏周边地区的风险;铣削时旋转整个总成的风险;同时也存在被井下钻具组合(BHA)卡住的风险。铣磨干预方案的起草考虑了不同的情况,包括突发事件。由于作业的紧迫性和铣削后SSSV的高精度要求,E-line传输的机器人铣削干预是首选。机器人工具串首先用于下入。随后进行的诊断下入有助于团队了解井下情况,调整作业计划,并测试井下工具的性能。最后,磨铣作业在采集系统上显示了一个明确的签名,为相关各方提供了关于结果的确定性。进行了一次摄像机下入,以验证磨铣后作业区域的条件。根据程序,该作业总共运行了四次。此外,铣削时间本身仅为17分钟。在SSSV功能齐全的情况下,客户可以在测试完井的完整性后立即恢复生产。本文描述了一种复杂但高效的作业,通过电缆输送的机器人铣削工具能够消除关键的井下障碍,恢复生产,同时保持井的所有安全特征,从而避免了复杂的修井作业。经过深入的准备工作,然后有条不紊地执行,这口井恢复了石油生产。
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引用次数: 0
Lessons from High-Speed Data Acquisition on Frac Plug Milling Operations 高速数据采集在压裂桥塞磨铣作业中的应用
Pub Date : 2023-03-14 DOI: 10.2118/212904-ms
K. Newman, P. Kelleher
Previous work has shown that large force waves traveling through the coiled tubing (CT) correlated with extended reach tool (ERT) operations can generate axial vibration harmonics in the CT that may lead to CT failures. This paper documents continued work which has shown that the surface equipment also has natural frequencies of vibration. When these natural frequencies are multiples of the ERT frequency, the ERT stimulates the surface equipment vibration modes.
之前的研究表明,与大位移工具(ERT)作业相关的大力波穿过连续油管(CT),可能会在连续油管中产生轴向振动谐波,从而导致连续油管失效。本文记录了继续进行的工作,表明地面设备也具有固有振动频率。当这些固有频率是ERT频率的倍数时,ERT会刺激地面设备的振动模式。
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引用次数: 0
Protecting from H2S Damage – Expanding the Knowledge 防止H2S损害-扩展知识
Pub Date : 2023-03-14 DOI: 10.2118/212944-ms
S. Craig, B. Lindsey, K. Elliott, E. Arriaga, Finlay Thom, Anjan Blatter
This paper will present an update on the operational benefits of utilizing anti-cracking inhibitors in sour wells. Multiple papers have shared the details of a Joint Industry Project which resulted in a one-size-fits-all fatigue derating factor by the service supplier. In recent years, additional testing has challenged that practice and a greater variety of improved derating factors are utilized in fatigue tracking software. The testing process of exposing samples to sour conditions for 72 hours and conducting bend fatigue testing post exposure remains the method used in this paper. The process updated the JIP practice of one-time coating of the sample with the addition of an anti-cracking inhibitor to the sour fluid. This update more closely replicates real-world operations. In addition, there was a greater focus on the test sample size, stress and strain to reduce fatigue testing time and reduce the effects of any outgassing leading to a more accurate and repeatable test. A comparison of three typical test methods will be presented: non-inhibited sour tests by the original equipment manufacturer, inhibited field specific partial pressure testing by an operator and globally applicable inhibited testing conducted at the maximum apparatus test level by a service provider. Comparison of prior anti-cracking inhibitor and a North Sea approved inhibitor results will be detailed. The practice for conducting the tests with a high yield material and extending the results to a lower grade material with similar chemistry will be detailed. Note that the results of separate tests conducted on the pipe body and bias welds will be compared and detailed. A brief summary of the service providers record of global sour pipe operations will illustrate these practices have proved suitable in the field. The updated practices and procedures for sour testing have not been shared in prior papers. The improved pipe life will assist the industry with efficient and safe operational planning in sour wells. Finally extending pipe life will reduce the amount of raw steel required for operations and ultimately reducing carbon dioxide emissions, a global challenge from which we can all benefit.
本文将介绍在含酸井中使用抗裂化抑制剂的最新操作效益。多篇论文分享了一个联合行业项目的细节,该项目导致了服务供应商的一刀切的疲劳降额系数。近年来,额外的测试挑战了这种做法,并且在疲劳跟踪软件中使用了更多种类的改进降额因子。将试样置于酸性条件下72小时,并在暴露后进行弯曲疲劳试验的试验过程保持本文所采用的方法。该工艺更新了JIP的做法,即在酸性流体中添加抗裂解抑制剂,对样品进行一次性涂层。此更新更接近地复制了实际操作。此外,还更加关注测试样本大小、应力和应变,以减少疲劳测试时间,减少任何放气的影响,从而实现更准确和可重复的测试。将介绍三种典型测试方法的比较:原始设备制造商进行的非抑制酸性测试,操作人员进行的抑制现场特定分压测试以及服务提供商在最大设备测试水平上进行的全球适用的抑制测试。将详细比较先前的抗裂抑制剂和北海批准的抑制剂的结果。将详细介绍用高收率材料进行试验并将结果扩展到具有相似化学性质的较低等级材料的做法。请注意,将对管体和偏置焊缝进行单独测试的结果进行比较和详细说明。通过对服务提供商全球酸管作业记录的简要总结,可以说明这些方法在现场是适用的。在以前的论文中没有分享酸试验的最新实践和程序。延长的管柱寿命将有助于行业在含酸井中制定高效、安全的作业计划。最后,延长管道寿命将减少作业所需的原钢量,并最终减少二氧化碳排放,这是一个全球性的挑战,我们都可以从中受益。
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引用次数: 0
Interventions in High Cross-Flow / Auto Gas Lift Well in Chirag Field, Caspian Region 里海地区Chirag油田高横流/自动气举井干预措施
Pub Date : 2023-03-14 DOI: 10.2118/212929-ms
R. Adilov, R. Karimova, Javid Aliyev
This paper presents the intervention activities performed under high crossflow conditions in Chirag Auto Gas Lift (In-situ GL/Natural GL) completion design where crossflow between the reservoir zones posed a major challenge. Auto Gas Lift design was installed on a few selected wells of the Chirag field due to a lack of conventional gas-lift equipment, compressors, and pipelines. When Auto gas lift wells are shut in, crossflow occurs between the high-pressure gas-bearing zone used to lift the oil and the lower- pressured oil-bearing reservoir zone. The amount of crossflow is controlled by installing a choke (gas lift valve) across the gas bearing zone. On well A completed in August 2020, an oversize Gas Lift Valve was installed which created suboptimal flowing conditions, production deferrals and severe crossflow during shut-in. An intervention activity was carried out to replace the oversized valve in this severe crossflow condition. Installation of a plug was necessary to stop the cross-flow during the valve change-out operation but proved to be very challenging because the force from the crossflow - a rushing mixture of gas/sand - would be pushing against the cross-sectional area of any tool that is to be RIH. This paper describes the multiple options that can be worked out via modelling to define the optimal approach for successful intervention operations in high crossflow environments. The rate of cross-flow in the well can limit well intervention options. Due to piston force created by cross- flow, conventional methods of reservoir isolation are not always feasible, hence deployment method needs to be thoroughly analyzed during job planning. Several ways of reservoir isolation methods – utilizing slickline or e-line methodology have been cross-checked through rigorous modelling and collaboration with the contractors. This modelling revealed that well A crossflow conditions exceeded the safe operating limits of the Slickline wire and would introduce significant damages to the e-line wire due to the build-up piston force on the plug as it expands. After a few iterations, the optimized solution was identified as having an anchor that would be set before the plug and allow the passage of the gas flow through it. This intervention activity was carried out successfully on Well A as a result of the mutual efforts of all partners. The article also discusses the option of killing the well as a last resort to proceed with a required intervention job.
本文介绍了在齐拉格自动气举(原位GL/天然GL)完井设计中,在高交叉流条件下进行的修井活动,其中储层之间的交叉流是一个主要挑战。由于缺乏传统气举设备、压缩机和管道,在Chirag油田的几口选定的井中安装了自动气举设计。自动气举井关井时,用于采油的高压含气层与低压含油储层之间会发生横流。通过在含气区安装节流器(气举阀)来控制横流的量。在2020年8月完成的A井上,安装了一个超大尺寸的气举阀,造成了不理想的流动条件、生产延迟和关井期间严重的过流。在这种严重的横流情况下,进行了干预活动以更换过大的阀门。在更换阀门的过程中,必须安装堵头来阻止交叉流动,但事实证明这是非常具有挑战性的,因为来自交叉流动的力量——一种快速的气体/砂混合物——将推动任何RIH工具的横截面。本文描述了可以通过建模来确定在高横流环境中成功进行修井作业的最佳方法的多种选择。井内的过流速率会限制油井干预措施的选择。由于横向流动产生的活塞力,传统的储层隔离方法并不总是可行的,因此在作业规划时需要对部署方法进行深入的分析。通过严格的建模和与承包商的合作,对几种储层隔离方法(利用钢丝绳或e-line方法)进行了反复验证。该模型显示,A井的横流条件超过了钢丝绳的安全使用极限,并且由于桥塞膨胀时活塞力的累积,会对电缆造成严重损害。经过几次迭代,优化的解决方案被确定为具有一个锚点,可以在桥塞之前坐封,并允许气体流过它。在所有合作伙伴的共同努力下,A井的修井作业取得了成功。文章还讨论了将压井作为进行所需修井作业的最后手段的选择。
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引用次数: 0
The Vital Role of Well Intervention Technologies and Techniques in Pushing the Boundaries in Extreme Well Completions 修井技术和技术在极端完井中突破界限的重要作用
Pub Date : 2023-03-14 DOI: 10.2118/212928-ms
Laurie S. Duthie, Muhammad Awwadh Harthi, Hussain Saiood, O. Afif
The advantages of drilling extended reach wells (ERW’s) are well known; increased reservoir contact, reduced surface footprint and less wells drilled. Although the benefits of drilling these wells is clear, it is also essential to have the ability to conduct well intervention throughout the life of the well. Matrix acid stimulation and production logging are critically important well intervention operations for efficient reservoir management. Coiled tubing (CT) is commonly deployed in ERW’s to perform these intervention operations. For open hole ERW’s, the success of the operation is often directly correlated to the length of the lateral covered. For ERW’s that can exceed 30,000 ft, the challenges to reach total depth (TD) can almost be insurmountable in terms of overcoming the high frictional forces acting against the CT. The level of difficulty is further magnified covering open sections often greater than 10,000 ft, where additional frictional forces are present from the rock, high dogleg severity and well trajectory. High bottom hole temperature along with high H2S & CO2 levels pose further challenges. Formation damage after drilling may result in serious production and therefore economic consequences and it is imperative to restore reservoir permeability along the complete interval with accurate treatment placement. The same challenges are present for logging operations where the main objective is to determine the flow profile along the entire open hole section. To achieve the main objectives, a comprehensive approach is taken for these well intervention operations. Custom designed technologies have been developed to increase the open hole coverage achieved to provide good zonal coverage in matrix acid treatments and also a clearer understanding of multiphase flow from the formation during production logging. Technologies developed specifically to tackle these challenges are hydraulically powered CT tractors that can deliver up to 14,000 lbs pulling force and mechanical agitator tools that effectively reduce the total friction coefficient. Other technologies employed are a downhole compression/tension sub to monitor downhole performance in real time to enhance operational decision making. To extend the ultimate reach, certain techniques can add a few thousand feet in coverage. These techniques include high pressure jetting to clean out the horizontal section of the cased hole to lower the friction, strategically deploying friction reducer and using momentum assiduously. These new technologies and applied techniques opens the window to ultimately meeting the goals of improved well surveillance and treatment in long horizontal laterals. Creative solutions have been core to inventing the best fit for purpose technologies, with great leaps having been made through pioneering technologies to extend CT reach in these extreme conditions.
大位移井(ERW’s)的优势是众所周知的;增加了储层接触,减少了地面占地面积,减少了钻井数量。虽然钻井这些井的好处是显而易见的,但在井的整个生命周期内,有能力进行油井干预也是至关重要的。为了实现高效的储层管理,基质酸化和生产测井是至关重要的修井作业。连续油管(CT)通常部署在ERW中进行这些修井作业。对于裸眼ERW,作业的成功与否通常与分支覆盖的长度直接相关。对于长度超过30,000英尺的ERW,达到总深度(TD)的挑战几乎是无法克服的,因为要克服作用于连续油管的高摩擦力。对于通常大于10,000英尺的开放段,难度进一步加大,因为岩石、狗腿的严重程度和井眼轨迹都存在额外的摩擦力。井底温度高,H2S和CO2含量高,这些都是进一步的挑战。钻井后的地层损害可能会导致严重的生产和经济后果,因此必须通过精确的处理位置来恢复整个层段的储层渗透率。测井作业也面临着同样的挑战,测井作业的主要目标是确定整个裸眼段的流动剖面。为了实现主要目标,这些修井作业采用了综合方法。开发了定制设计的技术,以增加裸眼覆盖范围,在基质酸处理中提供良好的层间覆盖,并在生产测井过程中更清楚地了解地层的多相流。为了应对这些挑战,专门开发了液压驱动的连续油管牵引器(可提供高达14000磅的拉力)和机械搅拌工具(可有效降低总摩擦系数)。采用的其他技术包括井下压缩/张力短节,用于实时监测井下性能,以提高作业决策。为了扩大最终覆盖范围,某些技术可以增加几千英尺的覆盖范围。这些技术包括高压喷射,以清洁套管井的水平段,以降低摩擦,策略性地部署摩擦减速器,并努力使用动量。这些新技术和应用技术为最终实现改进长水平分支井的监测和处理目标打开了一扇窗。创新的解决方案是发明最适合用途的技术的核心,通过开创性的技术,扩大了CT在极端条件下的覆盖范围,取得了巨大的飞跃。
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引用次数: 1
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Day 1 Tue, March 21, 2023
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