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Petrophysical Evaluation of the Reservoir in the K - Field, Offshore Ghana 加纳近海K -油田储层岩石物性评价
Pub Date : 2019-08-05 DOI: 10.2118/198796-MS
Prosper Anumah, S. Mohammed, Justice Sarkodie-kyeremeh, W. N. Aggrey, Anthony Morgan
Reliable assessment of the petrophysical properties of hydrocarbon-bearing reservoirs is essential for the estimation of hydrocarbon reserves, identification of good production zones, and assessing the need for hydro-fracturing jobs. The K-Field although discovered in the 1970s is yet to be developed. In this study, well logs from the wells drilled in this field were analysed with the primary objective of determining the petrophysical properties of the reservoir zones using various estimation models. From the log readings, the reservoir sands containing hydrocarbons in the field are found to be located at the Mid Turonian (90Ma)-Intra Upper Albian (96.5Ma) and Intra Upper Albian (98Ma). The porosity was determined using the density log and crossplots. Archie and Simandoux correlations were utilized in the determination of the water saturation. Permeability was estimated using Timur, Tixer and Coates correlations. The findings after the petrophysical evaluation indicate that the wells entered formations with good reservoir quality in terms of porosity, which ranges from 16.12% to 20.97%. In relation to hydrocarbon saturation and permeability, two of the wells gave better results suggesting that they were drilled through the productive part of the reservoir. Nonetheless, the average permeability of the reservoir is estimated to be very low. This suggests that in the field development planning, well stimulation methods should be incorporated to aid the ability of the reservoir rocks to transmit fluids into the production wells.
对含油气储层的岩石物理性质进行可靠的评估对于估计油气储量、确定良好的生产区域以及评估水力压裂作业的必要性至关重要。k油田虽然在20世纪70年代被发现,但尚未得到开发。在本研究中,对该油田钻井的测井曲线进行了分析,主要目的是利用各种估计模型确定储层的岩石物理性质。根据测井数据,油田含烃储层砂位于中Turonian (90Ma)-Intra Upper Albian (96.5Ma)和Intra Upper Albian (98Ma)。孔隙度采用密度测井和正交图确定。利用Archie和Simandoux相关系数测定含水饱和度。渗透率采用Timur、Tixer和Coates相关性进行估算。岩石物性评价结果表明,该井进入的储层孔隙度为16.12% ~ 20.97%,储层质量较好。在油气饱和度和渗透率方面,其中两口井取得了较好的结果,表明它们钻穿了储层的生产部分。尽管如此,据估计该储层的平均渗透率非常低。这表明,在油田开发规划中,应结合油井增产措施,以提高储层岩石向生产井输送流体的能力。
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引用次数: 0
Gas Lift Optimization within Field Capacity Limitations 油田产能限制下的气举优化
Pub Date : 2019-08-05 DOI: 10.2118/198744-MS
Uche Chukwunonso Ifeanyi, Samuel Esieboma, Jennifer Uche
Optimizing oil production with facility constraints has become a challenge to most E&P companies even as they pursue sustainable resources. The innovative gas lift technique overcomes this challenge. The conventional gas lift well system has long been in use, but the design most times is limited by gas availability and pressure which limits the depth of gas lift injection for improved production rates. This challenge may not be evident in matured producing fields with gas compressors installed with available non-associated gas source wells, but truly such challenges arise in new fields especially owned by indigenous companies where much uncertainties at an early field life unavoidably allows you to be more stringent in expenditures towards development of a field gas lift project. A new gas lift concept was developed and studied in Field A in an offshore field of the Niger delta in the absence of gas compressors. This design has been proven to be suitable because it was used to bring four closed wells online even when those wells were removed from the company annual forecast. The original design consists of a minimum of two unloading valves and an orifice at a deeper depth, but because of the absence of scrubbers and gas compressors in the facility, pressure depletion in the reservoirs caused four flowing wells to be closed. The new design then sets dummy at shallow mandrels and uses a modified size of orifice to optimize available pressure and gas required to open the closed wells and still sustain other gas lifted wells connected to the same gas lift manifold. This campaign resulted to an additional 7000Bopd which is the primary discussion of this paper.
在设施限制的情况下优化石油产量已经成为大多数勘探开发公司面临的挑战,即使他们追求可持续资源。创新的气举技术克服了这一挑战。传统的气举井系统已经使用了很长时间,但大多数时候的设计受到气体可用性和压力的限制,这限制了气举注入的深度,以提高产量。这一挑战在成熟的生产油田中可能并不明显,因为这些油田安装了气体压缩机和可用的非伴生气源井,但在新油田,特别是本土公司拥有的新油田中,这种挑战确实会出现,因为这些油田早期的许多不确定性不可避免地会让你在开发气田气举项目时更加严格地控制支出。在尼日尔三角洲海上油田的A油田,在没有气体压缩机的情况下,开发和研究了一种新的气举概念。这种设计已被证明是合适的,因为它使4口关闭的井上线,即使这些井已从公司的年度预测中删除。最初的设计包括至少两个卸载阀和一个较深的孔板,但由于设施中没有洗涤器和气体压缩机,储层的压力耗尽导致4口流动井关闭。然后,新设计将假人设置在浅心轴上,并使用修改尺寸的孔板来优化打开关闭井所需的可用压力和气体,同时仍然维持连接到同一气举歧管的其他气举井。这一举措带来了额外的7000桶/天的产量,这是本文的主要讨论内容。
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引用次数: 2
Experimental Investigation of the Effects of Different Environmental Conditions on Pipelines Corrosion Rates 不同环境条件对管道腐蚀速率影响的实验研究
Pub Date : 2019-08-03 DOI: 10.2118/198708-MS
O. Adeyanju, L. Oyekunle
An estimate of about $18.5 million are expended by industries in Nigeria yearly on corrosion, the oil and gas industry takes more than 65% of this cost due to the peculiar nature of their facilities and operational conditions. In spite of the use of galvanized pipeline and application of the anti-corrosion coating of crude oil pipeline and other metallic structure in the oil and gas industry, corrosion failures are still daily occurrences. These corrosive failures have been attributed to the environmental conditions in which the pipeline and other metallic structures are located. This research studies the rate of deterioration (corrosion rate) of carbon steel pipeline (flow pipe) under five different environmental conditions, coated with different anti-corroding agents, and subjected to different temperatures and pH values. Five Different environmental conditions through which pipelines are laid (Top soil + Fresh water, Sea water bed sand + Sea water, Lagoon water, Seawater, NaCl solution (0.5M)) were simulated in the laboratory. Different seventy gram (70g) samples of the carbon steel pipeline were used as the coupon samples. Red oxide oil paint and tar paint were used as the anti-corroding agents. Water bath was used in regulating the temperature and different concentration of HCL and NaOH were used to vary the pH. Weight loss method was used to calculate the corrosion rates. Results show that carbon steel resists corrosion better when buried in soil than when submerged in water; also the corrosion rate is more in sea water than in the lagoon water of relatively smaller salinity. The rate of corrosion was observed to increase with: increase in temperature, increase in salinity, and increases in acidity and alkalinity. Also the tar paint is more effective as anti-corrodant than the red oxide oil paint when applied to the carbon steel pipeline under same environment conditions. The study successively reduced the corrosion rate of the 70g coupon sample from 0.00127g/day when the sample were suspended in 0.5M, NaCl solution to 0.000104g/day when pipeline coated with tar paint are buried in dry soil.
据估计,尼日利亚工业每年在腐蚀方面的支出约为1850万美元,由于石油和天然气行业设施和运营条件的特殊性,其成本占该成本的65%以上。尽管在石油和天然气工业中使用了镀锌管道,并在原油管道和其他金属结构上应用了防腐涂层,但腐蚀故障仍然是家常便饭。这些腐蚀失效归因于管道和其他金属结构所处的环境条件。本研究研究了碳钢管道(流管)在五种不同的环境条件下,涂有不同的防腐蚀剂,承受不同的温度和pH值时的劣化速率(腐蚀速率)。在实验室模拟了5种不同敷设管道的环境条件(表层土+淡水、海水床砂+海水、泻湖水、海水、0.5M NaCl溶液)。采用不同的70克(70g)碳钢管道样品作为试样。采用氧化红油漆和沥青漆作为防腐蚀剂。用水浴调节温度,用不同浓度的HCL和NaOH来改变ph值,用失重法计算腐蚀速率。结果表明:碳钢埋在土中比浸没在水中耐腐蚀性能好;海水中的腐蚀速率也高于盐度相对较小的泻湖水。腐蚀速率随温度的升高、盐度的升高、酸度和碱度的增加而增加。同样的环境条件下,沥青漆在碳钢管道上的防腐效果也优于氧化红漆。该研究将70g试样的腐蚀速率从悬浮在0.5M, NaCl溶液中的0.00127g/day降低到涂有沥青涂料的管道埋在干燥土壤中的0.000104g/day。
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引用次数: 0
Egina Deep Water Development: Isolation Barrier Valve Case Study Egina深水开发:隔离屏障阀案例研究
Pub Date : 2018-03-20 DOI: 10.4043/28453-MS
G. Forrest, Christophe Morand, Kenneth Johnson, V. Okengwu, V. Chaloupka
A major operator manages multiple deep water projects in the Gulf of Guinea. This paper describes the latest 44-well project in Nigeria. The operator required an ISO 28781 qualified bi-directional subsurface isolation barrier valve (IBV) (Fig. 1) to be installed in each well. This work presents results of IBV deployment in the field. The wells were drilled and completed from sixth generation drillships. To comply with the operator's dual barrier policy, a bi-directional IBV was installed in each well to help ensure reservoir isolation for temporary well suspension or before running upper completion and tree installation. Careful attention to well fluid cleanliness, sound quality assurance/quality control (QA/QC), and operational procedures were considered paramount to successful remote opening of the IBVs and were identified as best practices by both parties. The IBV is run in the open position as an integral part of the lower completion. A collet shifting tool closes the ball isolating the formation, enabling inflow and positive pressure testing to be performed. The reservoirs are isolated by the closed ball in the IBV, allowing safe installation of the upper completion from a floating rig or well suspension without a subsea tree. The use of an ISO 28781 Type CC V1 qualified IBV provides both zonal isolation and fluid-loss control. Once a well is completed and the subsea tree installed, the IBV is remotely functioned to the open position by applying multiple tubing pressure cycles. The first batch of wells were drilled and completed with lower completions and suspended while waiting for subsea tree deliveries. Later, wells were drilled and completed with both lower and upper completions, and trees were installed later from an offshore inspection maintenance and repair (OIMR) vessel. IBVs were successfully closed and inflow and pressure tested during the lower completion phase. IBVs are run in sieved non-aqueous based mud (NABM). Filtered high viscosity pills are spotted across the IBV before closing. Once closed, the casing above the IBV is displaced to filtered completion brine at a rate ensuring any debris is lifted to the surface. The wells remain suspended with IBVs closed until the operator performs flowback and injectivity testing from a drillship. Additional injectivity testing was also performed from an OIMR vessel. Well suspension duration with IBVs closed varied between two months and 2.5 years. All valves cycled opened without issues. Four coiled tubing (CT) interventions were performed in the field, passing through the open ball without issue, confirming the IBVs were in the fully open position. This paper describes full QA/QC and operational procedures, which led to successful deployment and excellent functionality of the IBVs.
一家大型运营商在几内亚湾管理着多个深水项目。本文介绍了尼日利亚最新的44口井项目。作业者要求在每口井中安装一个符合ISO 28781标准的双向地下隔离阀(IBV)(图1)。这项工作介绍了IBV在现场部署的结果。这些井是由第六代钻井船钻井和完井的。为了遵守运营商的双重隔离政策,在每口井中都安装了一个双向IBV,以帮助确保临时停井或下完井和采油树安装之前的油藏隔离。仔细关注井液清洁度、健全的质量保证/质量控制(QA/QC)和操作程序对于成功远程开启ibv至关重要,并被双方确定为最佳实践。IBV作为下部完井的一个组成部分,在打开位置下入。夹头移动工具关闭球体,隔离地层,从而进行流入和正压测试。储层由IBV中的封闭球隔离,无需海底采油树,即可通过浮式钻机或井悬架安全安装上部完井装置。使用符合ISO 28781 CC V1标准的IBV,可实现层间隔离和失液控制。一旦一口井完井,海底采油树安装完毕,IBV就会通过多个油管压力循环,远程启动到开启位置。第一批井以较低完井率钻完井,在等待海底采油树交付期间暂停作业。随后,下部和上部完井都进行了钻井和完井,随后通过海上检查维护和维修(OIMR)船安装了采油树。在下部完井阶段,ibv成功关闭,并进行了流入和压力测试。ibv在经过筛分的非水基泥浆(NABM)中下入。过滤后的高粘度药丸在IBV关闭前被发现。一旦关闭,IBV上方的套管将被置换到过滤过的完井盐水中,以确保任何碎屑被提至地面。在作业公司从钻井船上进行返排和注入测试之前,ibv关闭,井处于暂停状态。此外,还在OIMR容器上进行了额外的注入性测试。关闭ibv的停井时间从2个月到2.5年不等。所有阀门循环开启没有问题。在现场进行了四次连续油管(CT)干预,没有出现问题,通过开放的球,确认ibv处于完全打开的位置。本文描述了完整的QA/QC和操作过程,这些过程导致了ibv的成功部署和出色的功能。
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引用次数: 0
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Day 2 Tue, August 06, 2019
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