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Fatigue Fracture of a Cast Stainless Steel Lever 铸造不锈钢杠杆的疲劳断裂
Pub Date : 2019-06-01 DOI: 10.31399/asm.fach.aero.c0046142
To ensure no malfunctions and although there were no apparent problems, a main fuel control was returned to the factory for examination after service on a test aircraft engine that had experienced high vibrations. When the fuel control was disassembled, a lever, cast from AMS 5350 (AISI type 410) stainless steel that was through-hardened to 26 to 32 HRC and passivated, was shown to be cracked. The crack initiated at the sharp corner of the elongated milled slot and propagated across to the outer wall. The sections around the crack were spread about 30 deg apart, showing the fracture surface under investigation had beach marks initiating at the sharp corner along the milled slot. Changes in frequency or amplitude of vibration caused different rates of propagation, resulting in a change in pattern. This evidence supported the conclusion that the lever failed in fatigue as a result of excessive vibration of the fuel control on the test engine. Recommendations included redesign of the lever with a large radius in the corner where cracking originated. This would reduce the stress-concentration factor significantly, thus minimizing the susceptibility of the lever to fatigue.
为了确保没有故障,尽管没有明显的问题,但在对经历了高振动的测试飞机发动机进行服务后,一个主要的燃料控制被送回工厂进行检查。当燃料控制装置拆卸时,一根由AMS 5350 (AISI 410型)不锈钢铸造的杠杆,经过26至32 HRC的硬化和钝化,显示出裂纹。裂纹始于细长铣削槽的尖角,并向外壁扩展。裂缝周围的剖面间距约为30度,表明所调查的断裂面在沿铣削槽的尖角处有滩痕。振动频率或振幅的变化引起不同的传播速率,从而导致图案的变化。这一证据支持了杠杆在疲劳中失效的结论,这是由于测试发动机上燃油控制装置的过度振动造成的。建议包括重新设计的杠杆与大半径的角落,开裂的起源。这将显著降低应力集中系数,从而最大限度地减少杠杆对疲劳的敏感性。
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引用次数: 0
Probabilistic Damage Tolerance Analysis of Gas Turbine Rotors 燃气轮机转子概率损伤容限分析
Pub Date : 2019-06-01 DOI: 10.31399/asm.fach.aero.c0090030
A DC-10 in transit from Denver to Chicago experienced failure of the center engine. The titanium compressor disk burst and severed the hydraulics of the plane. Investigation supports the conclusion that the cause of the disk rupture was the presence of a large fatigue crack near the bore emanating from a hard alpha (HA) defect. Such defects can result from occasional upsets during the vacuum melting of titanium. These nitrogen-rich alpha titanium anomalies are brittle and often have associated microcracks and microvoids. A probabilistic damage tolerance approach was recommended to address the anomalies, with the objective of enhancing rotor life management practices. The ongoing work involves the use of fracture mechanics and software (called DARWIN.) optimized for damage tolerant design and analysis of metallic structural components.
一架DC-10在从丹佛飞往芝加哥的途中,中央引擎出现故障。钛合金压气机盘爆裂,切断了飞机的液压系统。调查支持的结论是,磁盘破裂的原因是存在一个大的疲劳裂纹附近的孔发出的硬α (HA)缺陷。这种缺陷可能是由于钛在真空熔化过程中偶尔发生的扰动造成的。这些富氮α -钛异常是脆性的,通常伴有微裂纹和微空洞。提出了一种概率损伤容限方法来解决异常问题,目的是提高转子寿命管理实践。正在进行的工作包括使用断裂力学和软件(称为DARWIN)来优化金属结构部件的损伤容忍度设计和分析。
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引用次数: 0
Failure of an Aircraft Controller Diaphragm 飞机控制器隔膜故障
Pub Date : 2019-06-01 DOI: 10.31399/asm.fach.aero.c0006394
A preflight inspection found a broken diaphragm from a side controller fabricated from 17-7 PH stainless steel in the RH 950 heat treatment condition. Failure occurred by cracking of the base of the flange-like diaphragm. The crack traveled 360 deg around the diaphragm. Scanning electron microscopy (SEM) revealed that the failure occurred by a brittle intergranular mechanism and stress-corrosion cracking (SCC), and indicated a failure mode of selective grain-boundary separation. The diaphragms were heat treated in batches of 25. An improper heat treatment could have resulted in the formation of grain boundary precipitates, including chromium carbides. It was concluded that failure of the diaphragm was due to a combination of sensitization caused by improper heat treatment and subsequent SCC. It was recommended that the remaining 24 sensor diaphragms from the affected batch be removed from service. In addition, a sample from each heat treat batch should be submitted to the Strauss test (ASTM A262, practice E) to determine susceptibility to intergranular corrosion. Also, it was recommended that a stress analysis be performed on the system to determine whether a different heat treatment (which would offer lower strength but higher toughness) could be used for this part.
飞行前检查发现,在RH 950热处理条件下,由17-7 PH不锈钢制成的侧控制器的隔膜破裂。失效是由于法兰式隔膜底部的开裂造成的。裂缝沿隔膜呈360度旋转。扫描电镜(SEM)分析表明,其破坏机制为脆性晶间破坏和应力腐蚀破坏,破坏模式为选择性晶界分离。膜片每批热处理25个。不适当的热处理可能导致晶界沉淀的形成,包括碳化铬。结论是膜片的失效是由于不适当的热处理和随后的SCC引起的敏化的结合。建议从受影响的批次中取出剩余的24个传感器隔膜。此外,每个热处理批次的样品应提交施特劳斯测试(ASTM A262,实践E),以确定对晶间腐蚀的敏感性。此外,建议对系统进行应力分析,以确定是否可以对该部件使用不同的热处理(强度较低但韧性较高)。
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引用次数: 0
Fatigue Cracking That Originated at a Material Defect in a Forged Aircraft Wheel Half 由锻造飞机轮毂半部分的材料缺陷引起的疲劳裂纹
Pub Date : 2019-06-01 DOI: 10.31399/asm.fach.aero.c0047125
A commercial aircraft wheel half, machined from an aluminum alloy 2014 forging that had been heat treated to the T6 temper, was removed from service because a crack was discovered in the area of the grease-dam radius during a routine inspection. Neither the total number of landings nor the roll mileage was reported, but about 300 days had elapsed between the date of manufacture and the date the wheel was removed from service. The analysis (visual inspection, macrographs, micrographs, electron microprobe) supported the conclusions that the wheel half failed by fatigue. The fatigue crack originated at a material imperfection and progressed in more than one plane because changes in the direction of wheel rotation altered the direction of the applied stresses. Recommendations included rewriting the inspection specifications to require sound forgings.
一架商用飞机的轮毂一半是由2014年的铝合金锻件加工而成,经过热处理至T6回火,由于在例行检查中发现油坝半径区域存在裂纹,因此被停止使用。着陆的总次数和滚转里程都没有报告,但是从制造日期到轮子停止使用的日期已经过去了大约300天。分析(目视、宏观、显微、电子探针)支持了车轮半失效的结论。由于车轮旋转方向的改变改变了施加应力的方向,疲劳裂纹起源于材料缺陷,并在多个平面上发展。建议包括重新编写检验规范,要求锻件声音良好。
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引用次数: 0
Failure of Steel Missile Launcher Attachment Bolts 钢质导弹发射装置连接螺栓失效
Pub Date : 2019-06-01 DOI: 10.31399/asm.fach.aero.c9001907
M. Pepi
Aircraft missile launcher attachment bolts fabricated from cadmium-coated Hy-tuf steel were found broken. Subsequent analysis of the broken bolts indicated three causes of failure. First, the bolts had been carburized, which was not in conformance with the heat treating requirements. Second, macroetching showed that the bolts has been machined from stock rather than forged, and the threads cut rather than rolled. It was also determined that hydrogen-assisted stress-corrosion cracking also played a part in the failure of the high-strength bolts.
用涂镉的Hy-tuf钢制造的飞机导弹发射装置连接螺栓被发现断裂。随后对断裂螺栓的分析指出了三个失效原因。一是螺栓渗碳,不符合热处理要求。其次,宏观蚀刻表明螺栓是机加工而不是锻造的,螺纹是切割而不是轧制的。还确定氢辅助应力腐蚀开裂也是导致高强度螺栓失效的原因之一。
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引用次数: 0
Stress-Corrosion Cracking of a Forged Aircraft Lug 锻造飞机凸耳的应力腐蚀开裂
Pub Date : 2019-06-01 DOI: 10.31399/asm.fach.aero.c0091678
During a routine shear-pin check, the end lug on the barrel of the forward canopy actuator on a naval aircraft was found to have fractured. The lug was forged from aluminum alloy 2014-T6. Investigation (visual inspection, 2x views, and 140X micrographs etched with Keller's reagent) supported the conclusion that the cause of failure was SCC resulting from exposure to a marine environment. The fracture occurred in normal operation at a point where damage from pitting and intergranular corrosion acted as a stress raiser, not because of overload. The pitting and intergranular attack on the lug were evidence that the surface protection of the part had been inadequate as manufactured or had been damaged in service and not properly repaired in routine maintenance. Recommendations included anodizing the lug and barrel in sulfuric acid and giving them a dichromate sealing treatment, followed by application of a coat of paint primer. During routine maintenance checks, a careful examination was suggested to look for damage to the protective coating, and any necessary repairs should be made by cleaning, priming, and painting. Severely corroded parts should be removed from service.
在一次常规的剪切销检查中,一架海军飞机的前舱盖执行器的桶上的端耳被发现断裂。耳片由2014-T6铝合金锻造而成。调查(目视检查,2x视图和140X显微镜蚀刻凯勒试剂)支持了失败的原因是由于暴露在海洋环境中导致的SCC的结论。在正常运行中,断裂发生在点蚀和晶间腐蚀造成的损伤产生应力的地方,而不是因为过载。凸耳上的点蚀和晶间侵蚀表明零件的表面保护在制造时不够充分,或者在使用中损坏,在日常维护中没有得到适当的修复。建议包括在硫酸中阳极氧化耳耳和桶,并给予重铬酸盐密封处理,然后涂上一层底漆。在日常维护检查中,建议仔细检查保护涂层是否损坏,任何必要的修复都应通过清洁、底漆和油漆进行。严重腐蚀的部件应该停止使用。
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引用次数: 0
Failure of Tool Steel Pylon Attachment Stud 工具钢塔连接螺柱失效
Pub Date : 2019-06-01 DOI: 10.31399/asm.fach.aero.c0006436
A failed H-11 tool steel pylon attachment stud was found during a routine walk-around inspection. The stud exhibited gross localized corrosion pitting at several different areas on its surface. Light general rust was also evident. Severe pitting occurred near the fracture location. The fracture face contained evidence of intergranular SCC as well as ductile dimples. The protective coating was found to be an inorganic water-base aluminide coating having a coating thickness of 7.5 to 13 micron (0.3 to 0.5 mil). The coating was of a nonuniform mottled nature. It was concluded that the failure of the pylon attachment stud was caused by general corrosion followed by SCC. The stud was not adequately protected against corrosion by the coating. It was recommended that the coating be applied to a thickness of 38 to 75 micron (1.5 to 3 mil) to provide long-time corrosion resistance. The coating must be either burnished or cured at 540 deg C (1000 deg F) to provide cathodic protection to the steel. Other coatings, such as cadmium or aluminum, were also recommended if a thinner coating is needed.
在例行巡视检查中发现H-11工具钢塔连接螺栓失效。螺柱在其表面的几个不同区域显示出明显的局部腐蚀点。轻微的铁锈也很明显。在断口附近发生了严重的点蚀。断裂面包含晶间SCC和韧性韧窝的证据。发现保护涂层为无机水基铝化物涂层,涂层厚度为7.5至13微米(0.3至0.5密耳)。涂层呈不均匀的斑驳状。分析认为,塔架连接螺柱的破坏是由普遍腐蚀引起的,其次是SCC。螺柱没有被涂层充分保护以防止腐蚀。建议涂层的厚度为38至75微米(1.5至3密耳),以提供长期耐腐蚀性。涂层必须在540摄氏度(1000华氏度)下抛光或固化,以对钢提供阴极保护。如果需要较薄的涂层,也建议使用其他涂层,如镉或铝。
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引用次数: 0
Fatigue Fracture of an Aluminum Alloy 7075-T73 Landing-Gear Torque Arm 7075-T73铝合金起落架扭矩臂的疲劳断裂
Pub Date : 2019-06-01 DOI: 10.31399/asm.fach.aero.c0046146
The torque-arm assembly (aluminum alloy 7075-T73) for an aircraft nose landing gear failed after 22,779 simulated flights. The part, made from an aluminum alloy 7075-T73 forging, had an expected life of 100,000 simulated flights. Initial study of the fracture surfaces indicated that the primary fracture initiated from multiple origins on both sides of a lubrication hole that extended from the outer surface to the bore of a lug in two cadmium-plated flanged bushings made of copper alloy C63000 (aluminum bronze) that were press-fitted into each bored hole in the lug. Sectioning and 2x metallographic analysis showed small fatigue-type cracks in the hole adjacent to the origin of primary fracture. Hardness and electrical conductivity were typical for aluminum alloy 7075. This evidence supported the conclusion that the arm failed in fatigue cracking that initiated on each side of the lubrication hole since no material defects were found at the failure origin. Recommendations included redesign of the lubrication hole, shot peeing of the faces of the lug for added resistance to fatigue failure, and changing of the forging material to aluminum alloy 7175-T736 for its higher mechanical properties.
一架飞机前起落架的扭力臂组件(7075-T73铝合金)在22,779次模拟飞行后失效。该部件由7075-T73铝合金锻件制成,预计使用寿命为10万次模拟飞行。对裂缝表面的初步研究表明,主要裂缝是从润滑孔两侧的多个起点开始的,润滑孔从外表面延伸到凸耳的孔,两个镀镉的法兰衬套由C63000铜合金(铝青铜)制成,压入凸耳的每个钻孔孔中。断面和2倍金相分析表明,在原生断口附近的孔洞中存在细小的疲劳型裂纹。硬度和电导率是铝合金7075的典型。这一证据支持了这样的结论:由于在失效原点处没有发现材料缺陷,因此在润滑孔的每一侧都开始出现疲劳裂纹,因此臂失效。建议包括重新设计润滑孔,对凸耳表面进行喷砂以增加抗疲劳失效的能力,并将锻造材料改为7175-T736铝合金,以获得更高的机械性能。
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引用次数: 0
Analysis of Aircraft Damage from a Lightning Strike 雷击对飞机损伤的分析
Pub Date : 2019-06-01 DOI: 10.31399/asm.fach.aero.c9001529
L. M. Gammon, M. Hyatt, G. H. Narayanan, H. Oberson, Harcayal B. Singh
On 16 July 1999, a Boeing 737-800 on final approach for landing sustained a major lightning strike. Damage to the fuselage structure primarily was in the form of melting or partial melting of widely-separated rivets and adjacent Alclad 2024-T3 fuselage skin. The damage was confined to a 0.25-in. (6.4-mm) radii around the affected rivets. The repair process involved removal of the locally-affected material and addition of a skin doubler to restore the aircraft structure to the originally designed condition. Damage features are described briefly.
1999年7月16日,一架波音737-800在最后进近准备着陆时遭遇了一次大雷击。机身结构损坏主要表现为大间距铆钉和相邻Alclad 2024-T3机身蒙皮熔化或部分熔化。损坏范围限制在0.25英寸。(6.4 mm)半径在受影响的铆钉周围。修复过程包括去除局部受影响的材料,并添加皮肤加倍剂,以将飞机结构恢复到最初设计的状态。简要描述了损伤特征。
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引用次数: 0
Fuel Line Corrosion 燃油管路腐蚀
Pub Date : 2019-06-01 DOI: 10.31399/asm.fach.aero.c0006398
Inspections and microstructural analysis revealed intergranular corrosion of 6061-T6 aluminum alloy aircraft fuel line beneath ferrules. The cause of the corrosion was traced to the fuel line marking process, which involved electrolytic labeling. Although subsequent rinsing of the fuel lines washed off most of the electrolyte, some was trapped between the 6061-T6 tubing and the ferrule. This condition made intergranular corrosion of the fuel lines inevitable. The attack caused grains to become dislodged, giving the appearance of pitting. Corrosion penetrated approximately 0.13 mm (0.005 in.) into the tubing. Experiments indicated that the corrosion products were inactive. It was recommended that another marking process be used that does not involve corrosive materials. The prevention of electrolyte from being trapped between the tubing and ferrules by using a MIL-S-8802 sealant was recommended.
检查和显微组织分析发现6061-T6铝合金飞机燃油管路在卡箍下存在晶间腐蚀。腐蚀的原因可以追溯到燃料管线标记过程,其中涉及电解标记。尽管随后的燃油管路冲洗掉了大部分电解液,但仍有一些被困在6061-T6油管和卡箍之间。这种情况使燃料管路的晶间腐蚀不可避免。这种攻击导致颗粒位移,产生点蚀现象。腐蚀渗入油管约0.13毫米(0.005英寸)。实验表明,腐蚀产物无活性。建议采用另一种不涉及腐蚀性材料的标记工艺。建议使用MIL-S-8802密封胶防止电解液被困在管道和卡箍之间。
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引用次数: 0
期刊
ASM Failure Analysis Case Histories: Air and Spacecraft
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