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Fracture of a Cast Stainless Steel Lever Because of a Cold Shut 铸造不锈钢拉杆因冷关闭而断裂
Pub Date : 2019-06-01 DOI: 10.31399/asm.fach.aero.c0089563
A lever (machined from a casting made of AISI type 410 stainless steel, then surface hardened by nitriding) that was a component of the main fuel-control linkage of an aircraft engine fractured in flight after a service life of less than 50 h. Investigation (radiographic inspection) supported the conclusions that the lever broke at a cold shut extending through approximately 95% of the cross section. The normally applied load constituted an overload of the remainder of the lever. Recommendations included adding magnetic-particle inspection to the inspection procedures for this cast lever.
飞机发动机主要燃油控制连杆部件的杠杆(由AISI 410型不锈钢铸件加工,然后通过氮化表面硬化)在飞行中断裂,使用寿命不到50小时。调查(射线检查)支持的结论是,杠杆在冷关闭时断裂,延伸到大约95%的横截面。正常施加的载荷构成了杠杆剩余部分的过载。建议包括在这个铸造杠杆的检查程序中增加磁粉检查。
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引用次数: 0
Use of Electron Fractography to Diagnose Hairline Cracking in an AISI 4340 Main Landing Gear Cylinder 用电子断口分析诊断AISI 4340主起落架油缸发际裂纹
Pub Date : 2019-06-01 DOI: 10.31399/asm.fach.aero.c9001540
J. A. Scott
Ground maintenance personnel discovered hydraulic fluid leaking from two small cracks in a main landing gear cylinder made from AISI 4340 Cr-Mo-Ni alloy steel. Failure of the part had initiated on the ID of the cylinder. Numerous cracks were found under the chromium plate. A 6500x electron fractograph showed cracking was predominantly intergranular with hairline indications. Leaking had occurred only 43 h after overhaul of the part. Total service time on the part was 9488 h. It was concluded that cracking on the ID was caused by hydrogen embrittlement which occurred during or after overhaul. The specific source of hydrogen which produced failure was not ascertainable.
地面维修人员发现,由美国AISI 4340 Cr-Mo-Ni合金钢制成的主起落架气缸有两个小裂缝,液压油从裂缝中泄漏。零件的故障是由气缸的内径引起的。在铬板下面发现了许多裂纹。6500x电子断口显示裂纹主要是沿晶断裂,有发际迹象。该部件在大修后仅43小时就发生了泄漏。零件的总使用时间为9488 h,内径开裂是由大修期间或大修后发生的氢脆引起的。产生故障的氢的具体来源不能确定。
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引用次数: 0
Fatigue Failure of a Steel Channel-Shaped Retainer Because of Vibration 一种槽钢保持架的振动疲劳失效
Pub Date : 2019-06-01 DOI: 10.31399/asm.fach.aero.c0047059
The governor on an aircraft engine failed and upon disassembly of the unit, it was discovered that the retainer for the flyweight pivot pins was broken. The channel-shaped retainer was made of 0.8 mm (0.030 in.) thick 1018 or 1020 steel. The part was plated with copper, which acted as a stop-off during carburizing of the offset, circular thrust-bearing surface surrounding the 16-mm (0.637-in.) diam hole. The bearing surface was case hardened to a depth of 0.05 to 0.1 mm (0.002 to 0.005 in.), then austempered to obtain a minimum hardness of 600 Knoop (1-kg, or 2.2-lb, load). Considerable vibration was created in the installation because of the design of the mechanical device used to transmit power to the governor. The pins were permitted to slide axially a small distance. Analysis (visual inspection, microscopic examination, and ductility measurements) supported the conclusion that failure of the retainer was the result of fatigue caused by vibration in the flyweight assembly. Impact of the pivot pins on the retainer also contributed to failure. Recommendations included redesign of the flyweight assembly, and replacement of the channel-shaped retainer with a spring-clip type of pin retainer.
一架飞机发动机上的调速器出现故障,在拆卸该装置时,发现飞重枢轴销的保持器坏了。槽形的保持器由0.8毫米(0.030英寸)厚的1018或1020钢制成。该部件镀上了铜,在对16毫米(0.637英寸)直径孔周围的圆形推力轴承表面进行渗碳时起到了阻止作用。轴承表面淬火至0.05至0.1毫米(0.002至0.005英寸)的深度,然后回火以获得600努(1公斤,或2.2磅,负载)的最小硬度。由于用于向调速器传递动力的机械装置的设计,在安装过程中产生了相当大的振动。销被允许轴向滑动一小段距离。分析(目视检查、显微检查和延性测量)支持以下结论:保持器的失效是由飞重组件振动引起的疲劳造成的。枢轴销对保持器的冲击也导致了失败。建议包括重新设计飞重总成,用弹簧夹型销保持器替换沟道形保持器。
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引用次数: 0
Failure of Resistance Spot Welds in an Aircraft Drop Tank Because of Poor Fit-Up 由于装配不良导致飞机油箱电阻点焊失效
Pub Date : 2019-06-01 DOI: 10.31399/asm.fach.aero.c0047673
A series of resistance spot welds joining Z-shape and C-shape members of an aircraft drop-tank structure failed during ejection testing. The members were fabricated of alclad aluminum alloy 2024-T62. The back surface of the C-shape members showed severe electrode-indentation marks off to one side of the spot weld, suggesting improper electrode contact. Visual examination of the weld fractures showed that the weld nuggets varied considerably in size, some being very small and three exhibiting an HAZ but no weld. Of 28 welds, only nine had acceptable nugget diameters and fusion-zone widths. The weld deficiencies were traced to problems in forming and fit-up of the C-shape members and to difficulties in alignment and positioning of the weld tooling. The failure of the resistance spot welds was attributed to poor weld quality caused by unfavorable fit-up and lack of proper weld-tool positioning. The problem could be solved by better forming procedures to provide an accurate fit-up that would not interfere with electrode alignment.
在弹射试验中,连接飞机弹射油箱z形和c形构件的一系列电阻点焊失效。构件材料为2024-T62铝合金。c形构件的背面在点焊的一侧显示出严重的电极压痕,表明电极接触不当。对焊缝断口的目视检查表明,焊缝掘进的大小变化很大,有些非常小,有三个表现出热影响区,但没有焊缝。在28个焊缝中,只有9个具有可接受的熔核直径和熔合区宽度。焊缝缺陷是由于c形构件的成形和装配问题以及焊接工装的对准和定位困难造成的。电阻点焊失效的主要原因是焊件装配不当和焊具定位不当导致焊缝质量差。这个问题可以通过更好的成形程序来解决,以提供精确的装配,而不会干扰电极对准。
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引用次数: 0
Fracture of a Landing-Gear Flat Spring 起落架扁平弹簧断裂
Pub Date : 2019-06-01 DOI: 10.31399/asm.fach.aero.c0048164
A flat spring for the main landing gear of a light aircraft failed after safe execution of a hard landing. The spring material was identified by chemical analysis to be 6150 steel. The fracture was found to have occurred near the end of the spring that was inserted through a support member about 25 mm thick and attached to the fuselage by a single bolt. Brinelling (plastic flow and indentation due to excessive localized contact pressure) was observed on the upper surface of the spring where the forward and rear edges of the spring contacted the support member. It was indicated by chevron marks that brittle fracture had started beneath the brinelled area at the forward edge of the upper surface of the spring. The origin of the brittle fracture was found to be a small fatigue crack that had been present for a considerable period of time before final fracture occurred. Fracture of the landing-gear spring was concluded to have been caused by a fatigue crack that resulted from excessive brinelling at the support point. Regular visual examinations to detect evidence of brinelling and wear at the support in aircraft with this configuration of landing-gear spring were recommended.
一架轻型飞机在安全执行硬着陆后,主起落架的扁平弹簧失效了。经化学分析,弹簧材料为6150钢。断裂发生在弹簧末端附近,弹簧插入一个约25毫米厚的支撑部件,通过一个螺栓连接在机身上。在弹簧的上表面,在弹簧的前后边缘与支撑构件接触的地方,观察到布林林现象(由于局部接触压力过大而产生的塑性流动和压痕)。从纹路的痕迹可以看出,在弹簧上表面前端边缘的边缘区域下,脆性断裂已经开始。脆性断裂的起源是一个小的疲劳裂纹,在最终断裂发生之前已经存在了相当长的一段时间。起落架弹簧断裂的原因是由于支撑点过度布氏而产生疲劳裂纹。建议使用这种起落架弹簧配置,定期进行目视检查,以检测飞机支承处的布氏磨损和磨损的证据。
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引用次数: 0
Fatigue Failure of an Aluminum Alloy Assembly at Spot Welds Because of Improper Heat Treatment 铝合金点焊件热处理不当导致的疲劳失效
Pub Date : 2019-06-01 DOI: 10.31399/asm.fach.aero.c0047072
Postflight inspection of a gas-turbine aircraft engine that had experienced compressor stall revealed that the engine air-intake bullet assembly had dislodged and was seated against the engine-inlet guide vanes at the 3 o'clock position. The bullet assembly consisted of an outer aerodynamic shell and an inner stiffener shell, both of 1.3 mm (0.050 in.) thick aluminum alloy 6061-T6, and four attachment clips of 1 mm (0.040 in.) thick alclad aluminum alloy 2024-T42. Each clip was joined to the outer shell by 12 spot welds and was also joined to the stiffener. Analysis (visual inspection, dye-penetrant inspection, and 10x/150x micrographs of sections etched with Keller's reagent) supports the conclusion that the outer shell of the bullet assembly separated from the stiffener because the four attachment clips fractured through the shell-to-clip spot welds. Fracture occurred by fatigue that initiated at the notch created by the intersection of the faying surfaces of the clip and shell with the spot weld nuggets. The 6061 aluminum alloy shell and stiffener were in the annealed (O) temper rather than T6, as specified. Recommendations included heat treating the shell and stiffener to the T6 temper after forming.
对一台经历过压气机失速的燃气涡轮飞机发动机的飞行后检查发现,发动机进气子弹组件已经脱落,并在发动机进气导叶的3点钟位置上。子弹组件包括一个外部气动外壳和一个内部加强壳,都是1.3毫米(0.050英寸)厚的6061-T6铝合金,以及四个1毫米(0.040英寸)厚的2024-T42铝合金附件夹。每个夹子通过12个点焊连接到外壳上,也连接到加强筋上。分析(目视检查、染料渗透检查和凯勒试剂蚀刻的10倍/150倍显微照片)支持这样的结论,即子弹组件的外壳与加强板分离,因为四个附件夹在壳与夹的点焊中断裂。断裂是由疲劳引起的,这种疲劳是由夹件和壳体表面与点焊块的交叉处产生的缺口引起的。6061铝合金外壳和加强筋采用退火(O)回火,而不是按照规定采用T6回火。建议包括热处理外壳和加强板到T6回火成形后。
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引用次数: 0
Failure Analysis of Silica Phenolic Nozzle Liners 二氧化硅酚醛喷嘴衬套失效分析
Pub Date : 2019-06-01 DOI: 10.31399/asm.fach.aero.c9001491
M. Katcher
Two silica phenolic nozzle liners cracked during proof testing. The test consisted of pressuring the nozzles to 14.1 MPa (2050 psia) for 5 to 20 s. It was concluded that the failure was due to longitudinal cracking in the convergent exhaust-nozzle insulators, stemming from the use of silica phenolic tape produced from flawed materials that went undetected by the quality control tests, which at the time, assessed tape strength properties in the warp rather than the bias direction. Once the nozzle manufacturer and its suppliers identified the problem, they changed their quality control procedures and resumed production of nozzle liners with more tightly controlled fiber/fabric materials.
两个二氧化硅酚醛喷嘴衬套在证明测试中破裂。试验包括将喷嘴加压至14.1 MPa (2050 psia) 5至20 s。结论是,故障是由于汇聚式排气喷嘴绝缘子的纵向开裂,这是由于使用了由有缺陷的材料生产的硅酚醛胶带造成的,而质量控制测试没有发现这些材料,当时的质量控制测试评估的是翘曲方向而不是偏倚方向的胶带强度特性。一旦喷嘴制造商及其供应商发现了这个问题,他们就改变了质量控制程序,并使用更严格控制的纤维/织物材料恢复了喷嘴衬套的生产。
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引用次数: 0
Analysis of Sub-Critical Cracking in a Ti-5Al-2.5Sn Liquid Hydrogen Control Valve Ti-5Al-2.5Sn液氢控制阀亚临界开裂分析
Pub Date : 2019-06-01 DOI: 10.31399/asm.fach.aero.c9001558
D. Meyn, R. Bayles
A liquid hydrogen main fuel control valve for a rocket engine failed by fracture of the Ti-5Al-2.5Sn body during the last of a series of static engine test firings. Fractographic, metallurgical, and stress analyses determined that a combination of fatigue and unexpected aqueous stress-corrosion cracking initiated and propagated the crack which caused failure. The failure analysis approach and its results are described to illustrate how fractography and fracture mechanics, together with a knowledge of the crack initiation and propagation mechanisms of the valve material under various stress states and environments, helped investigators to trace the cause of failure.
在一系列静态发动机点火试验的最后阶段,火箭发动机的液氢主燃料控制阀因Ti-5Al-2.5Sn阀体断裂而失效。断口学、冶金学和应力分析确定,疲劳和意外的水性应力腐蚀裂纹的结合引发并扩展了导致失效的裂纹。本文描述了失效分析方法及其结果,以说明断口学和断裂力学,以及对阀门材料在各种应力状态和环境下裂纹萌生和扩展机制的了解,如何帮助研究人员追踪失效原因。
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引用次数: 0
Failure of a Main Landing Gear on a Light Airplane 轻型飞机主起落架故障
Pub Date : 2019-06-01 DOI: 10.31399/asm.fach.aero.c9001018
C. Howard Craft
Initial investigation showed that a landing gear failure was the result of a hard landing with no evidence of contributory factors. The objective of reexamination was to determine whether there was any evidence of metallurgical failure. The landing gear was primarily an AISI type 6150 Cr-V steel flat spring attached at the top end to the fuselage and at the bottom end to the axle. Failure occurred at the clamping point near the top end of this spring. The failure showed evidence of severe brinelling at one corner in the clamping area. The fracture surfaces were clean, fresh, and indicative of a shock type of failure pattern. Closer examination, however, showed a fatigue crack at one corner. At this point, there was definite evidence of progression and oxidation. It was concluded that the corner in question was subjected to repeated brinelling resulting from normal landing loads, probably accentuated by looseness in the clamping device. The resulting residual tensile stress lowered the effective fatigue strength at that point against drag and side loads.
初步调查显示,起落架故障是硬着陆的结果,没有证据表明是其他因素造成的。复检的目的是确定是否有冶金失效的证据。起落架主要是一个AISI型6150 Cr-V钢扁平弹簧,连接在机身的顶部和轴的底部。故障发生在靠近弹簧顶端的夹紧点。故障显示在夹紧区域的一个角落有严重的布氏损伤的证据。断裂表面干净,新鲜,表明是一种冲击型的断裂模式。然而,更仔细的检查显示,在一个角落有疲劳裂纹。在这一点上,有明确的证据表明进展和氧化。得出的结论是,由于正常的着陆载荷,可能由于夹紧装置的松动而加剧了所讨论的角受到反复的压边。由此产生的残余拉伸应力降低了该点抗阻力和侧载荷的有效疲劳强度。
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引用次数: 0
Damaged Propeller Blades 螺旋桨叶片损坏
Pub Date : 2019-06-01 DOI: 10.31399/asm.fach.aero.c9001747
Jivan B. Shah
This report covers case histories of failures in fixed-wing light airplane and helicopter components. In a 2025-T6 or 2219 aluminum alloy propeller blade that failed near the tip, cracks started on the leading edge at surface damage in the critical area-the zone between 4 and 10 in. from the tip of the blade. Incorrect dressing and inadequate pre-flight inspection were the two main causes. Two other types of propeller blade fatigue failures resulted mainly from propeller straightening operations, usually performed after previous blade bending damage. To eliminate blade tip failures, all surface-damaged material should be removed and polished smooth before further flight. The blade should be correctly dressed. Also, the tachometer should be calibrated to ensure the engine/propeller combination is not operated in the critical speed range at normal cruising speeds.
本报告涵盖了固定翼轻型飞机和直升机部件故障的历史案例。在2025-T6或2219铝合金螺旋桨叶片中,在尖端附近发生故障时,在临界区域(4 - 10英寸)的前缘表面损伤处开始出现裂纹。从刀刃的尖端。不正确的着装和不充分的飞行前检查是两个主要原因。另外两种类型的螺旋桨叶片疲劳失效主要是由于螺旋桨矫直操作造成的,通常是在先前的叶片弯曲损伤之后进行的。为了消除叶尖故障,所有表面损坏的材料应在进一步飞行前去除并抛光光滑。刀刃应正确修整。此外,转速表应进行校准,以确保发动机/螺旋桨组合在正常巡航速度下不在临界速度范围内运行。
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引用次数: 0
期刊
ASM Failure Analysis Case Histories: Air and Spacecraft
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