Pub Date : 2019-06-01DOI: 10.31399/asm.fach.process.c0047161
Routine magnetic-particle inspection revealed crack indications in a number of shafts produced from hot-rolled 4130 steel bar. A pronounced indication of this size is cause for rejection if the defect is not eliminated during subsequent machining. A microstructural analysis of the shaft cross section revealed that the crack was approximately 0.5 mm (0.020 in.) deep and oriented in a radial direction. Furthermore, no stringer-type nonmetallic inclusions were observed in the vicinity of the flaw, which did not display the intergranular characteristics of a quench crack. The defect did, however, contain substantial amounts of oxide, which evidently resulted from the hot-working operation. This evidence supports the conclusion that the appearance of this discontinuity, with the long axis parallel to the working direction and radial orientation with regard to depth, strongly suggests a seam produced during rolling. Use of components with surface-defect indications as small as 0.5 mm (0.02 in.) can be risky in certain circumstances. Depending on the orientation of the flaw with respect to applied loads, the nature of the applied forces (for example, cyclic), and the operating environment, such a surface flaw can become the initiating site for a fatigue crack or a corrosion-related failure.
{"title":"Surface Indications in Hot-Rolled 4130 Steel Bars","authors":"","doi":"10.31399/asm.fach.process.c0047161","DOIUrl":"https://doi.org/10.31399/asm.fach.process.c0047161","url":null,"abstract":"\u0000 Routine magnetic-particle inspection revealed crack indications in a number of shafts produced from hot-rolled 4130 steel bar. A pronounced indication of this size is cause for rejection if the defect is not eliminated during subsequent machining. A microstructural analysis of the shaft cross section revealed that the crack was approximately 0.5 mm (0.020 in.) deep and oriented in a radial direction. Furthermore, no stringer-type nonmetallic inclusions were observed in the vicinity of the flaw, which did not display the intergranular characteristics of a quench crack. The defect did, however, contain substantial amounts of oxide, which evidently resulted from the hot-working operation. This evidence supports the conclusion that the appearance of this discontinuity, with the long axis parallel to the working direction and radial orientation with regard to depth, strongly suggests a seam produced during rolling. Use of components with surface-defect indications as small as 0.5 mm (0.02 in.) can be risky in certain circumstances. Depending on the orientation of the flaw with respect to applied loads, the nature of the applied forces (for example, cyclic), and the operating environment, such a surface flaw can become the initiating site for a fatigue crack or a corrosion-related failure.","PeriodicalId":294593,"journal":{"name":"ASM Failure Analysis Case Histories: Processing Errors and Defects","volume":"135 1","pages":"0"},"PeriodicalIF":0.0,"publicationDate":"2019-06-01","publicationTypes":"Journal Article","fieldsOfStudy":null,"isOpenAccess":false,"openAccessPdf":"","citationCount":null,"resultStr":null,"platform":"Semanticscholar","paperid":"126273559","PeriodicalName":null,"FirstCategoryId":null,"ListUrlMain":null,"RegionNum":0,"RegionCategory":"","ArticlePicture":[],"TitleCN":null,"AbstractTextCN":null,"PMCID":"","EPubDate":null,"PubModel":null,"JCR":null,"JCRName":null,"Score":null,"Total":0}
Pub Date : 2019-06-01DOI: 10.31399/asm.fach.process.c0047756
Waspaloy (AMS 5586) fabricated inner ring of a spray-manifold assembly failed transversely through the manifold tubing at the edge of the tube and support sleeve brazed joint. The assembly was brazed with AWS BAu-4 filler metal (AMS 4787). Fatigue beach marks propagating from extremities of a granular gold-tinted surface region adjacent to the tube-to-sleeve brazed joint and extending circumferentially were revealed by microscopic examination. Embrittlement of the tube caused by molten braze metal penetration along grain boundaries was evidenced by micrographs of a granular portion of the fracture. It was revealed by the initial fracture profile that fatigue cracks begun as an intergranular separation and subsequently became transgranular. It was concluded that failure of the tube was caused by excessive alloying between the braze metal and the Waspaloy. Reduced temperatures during torch debrazing or rebrazing were recommended to minimize molten braze metal penetration.
{"title":"Fatigue Fracture of Waspaloy Spray-Manifold Assembly Because of Embrittlement by Penetration of Molten Braze Metal","authors":"","doi":"10.31399/asm.fach.process.c0047756","DOIUrl":"https://doi.org/10.31399/asm.fach.process.c0047756","url":null,"abstract":"\u0000 Waspaloy (AMS 5586) fabricated inner ring of a spray-manifold assembly failed transversely through the manifold tubing at the edge of the tube and support sleeve brazed joint. The assembly was brazed with AWS BAu-4 filler metal (AMS 4787). Fatigue beach marks propagating from extremities of a granular gold-tinted surface region adjacent to the tube-to-sleeve brazed joint and extending circumferentially were revealed by microscopic examination. Embrittlement of the tube caused by molten braze metal penetration along grain boundaries was evidenced by micrographs of a granular portion of the fracture. It was revealed by the initial fracture profile that fatigue cracks begun as an intergranular separation and subsequently became transgranular. It was concluded that failure of the tube was caused by excessive alloying between the braze metal and the Waspaloy. Reduced temperatures during torch debrazing or rebrazing were recommended to minimize molten braze metal penetration.","PeriodicalId":294593,"journal":{"name":"ASM Failure Analysis Case Histories: Processing Errors and Defects","volume":"214 1","pages":"0"},"PeriodicalIF":0.0,"publicationDate":"2019-06-01","publicationTypes":"Journal Article","fieldsOfStudy":null,"isOpenAccess":false,"openAccessPdf":"","citationCount":null,"resultStr":null,"platform":"Semanticscholar","paperid":"122376480","PeriodicalName":null,"FirstCategoryId":null,"ListUrlMain":null,"RegionNum":0,"RegionCategory":"","ArticlePicture":[],"TitleCN":null,"AbstractTextCN":null,"PMCID":"","EPubDate":null,"PubModel":null,"JCR":null,"JCRName":null,"Score":null,"Total":0}
Pub Date : 2019-06-01DOI: 10.31399/asm.fach.process.c0048154
A medium-carbon helical spring was installed in a machine assembly that was welded into its final location. Weld spatter was not prevented from landing on the wire surface by any shield. An elongated drop and two tiny droplets of metal were observed a short distance from the fracture. No droplets were revealed at the origin of the fracture, but it was assumed that a drop of molten metal landed at the origin. Adherence of the spatter drop was expected to have been affected by the opening and closing of the fatigue crack. Weld spatter bead was concluded to have caused the fatigue fracture.
{"title":"Fatigue Failure Caused by Weld Spatter","authors":"","doi":"10.31399/asm.fach.process.c0048154","DOIUrl":"https://doi.org/10.31399/asm.fach.process.c0048154","url":null,"abstract":"\u0000 A medium-carbon helical spring was installed in a machine assembly that was welded into its final location. Weld spatter was not prevented from landing on the wire surface by any shield. An elongated drop and two tiny droplets of metal were observed a short distance from the fracture. No droplets were revealed at the origin of the fracture, but it was assumed that a drop of molten metal landed at the origin. Adherence of the spatter drop was expected to have been affected by the opening and closing of the fatigue crack. Weld spatter bead was concluded to have caused the fatigue fracture.","PeriodicalId":294593,"journal":{"name":"ASM Failure Analysis Case Histories: Processing Errors and Defects","volume":"7 1","pages":"0"},"PeriodicalIF":0.0,"publicationDate":"2019-06-01","publicationTypes":"Journal Article","fieldsOfStudy":null,"isOpenAccess":false,"openAccessPdf":"","citationCount":null,"resultStr":null,"platform":"Semanticscholar","paperid":"128112015","PeriodicalName":null,"FirstCategoryId":null,"ListUrlMain":null,"RegionNum":0,"RegionCategory":"","ArticlePicture":[],"TitleCN":null,"AbstractTextCN":null,"PMCID":"","EPubDate":null,"PubModel":null,"JCR":null,"JCRName":null,"Score":null,"Total":0}
Pub Date : 2019-06-01DOI: 10.31399/asm.fach.process.c0048124
Presence of transverse marks which were remnant of grinding was indicated in a failed valve spring made from ground rod. The shot-peening pattern was light at this location. A transverse crack was found to grow from one such mark under the influence of local stress fields until it was reoriented to the plane normal to the major tensile axis by sufficient loading. The shot-peening procedure was altered to create adequate surface compression at all stressed points on the springs.
{"title":"Failure of Valve Spring Because of Grinding and Shot Peening Operations","authors":"","doi":"10.31399/asm.fach.process.c0048124","DOIUrl":"https://doi.org/10.31399/asm.fach.process.c0048124","url":null,"abstract":"\u0000 Presence of transverse marks which were remnant of grinding was indicated in a failed valve spring made from ground rod. The shot-peening pattern was light at this location. A transverse crack was found to grow from one such mark under the influence of local stress fields until it was reoriented to the plane normal to the major tensile axis by sufficient loading. The shot-peening procedure was altered to create adequate surface compression at all stressed points on the springs.","PeriodicalId":294593,"journal":{"name":"ASM Failure Analysis Case Histories: Processing Errors and Defects","volume":"16 1","pages":"0"},"PeriodicalIF":0.0,"publicationDate":"2019-06-01","publicationTypes":"Journal Article","fieldsOfStudy":null,"isOpenAccess":false,"openAccessPdf":"","citationCount":null,"resultStr":null,"platform":"Semanticscholar","paperid":"128485651","PeriodicalName":null,"FirstCategoryId":null,"ListUrlMain":null,"RegionNum":0,"RegionCategory":"","ArticlePicture":[],"TitleCN":null,"AbstractTextCN":null,"PMCID":"","EPubDate":null,"PubModel":null,"JCR":null,"JCRName":null,"Score":null,"Total":0}
Pub Date : 2019-06-01DOI: 10.31399/asm.fach.process.c0047192
Fracture of a cadmium-plated accumulator ring forged from 4140 steel was discovered during inspection and disassembly of a hydraulic-accumulator system stored at a depot. The ring had broken into five small and two large segments. The small segments of the broken ring displayed very flat fracture surfaces with no apparent yielding, but the two large segments did show evidence of bending (yielding) near the fractures. In addition, some segments contained fine radial cracks. Analysis (visual inspection, optical microscopy on polished-and-etched specimens, hardness testing, and chemical analysis) supported the conclusion that the failure was caused due to brittle fatigue, as evidenced by the intergranular nature of the fracture path. Also, hydrogen penetration occurred during the plating operation and was not relieved subsequently as required.
{"title":"Fracture of an Accumulator Ring Due to Hydrogen Embrittlement","authors":"","doi":"10.31399/asm.fach.process.c0047192","DOIUrl":"https://doi.org/10.31399/asm.fach.process.c0047192","url":null,"abstract":"\u0000 Fracture of a cadmium-plated accumulator ring forged from 4140 steel was discovered during inspection and disassembly of a hydraulic-accumulator system stored at a depot. The ring had broken into five small and two large segments. The small segments of the broken ring displayed very flat fracture surfaces with no apparent yielding, but the two large segments did show evidence of bending (yielding) near the fractures. In addition, some segments contained fine radial cracks. Analysis (visual inspection, optical microscopy on polished-and-etched specimens, hardness testing, and chemical analysis) supported the conclusion that the failure was caused due to brittle fatigue, as evidenced by the intergranular nature of the fracture path. Also, hydrogen penetration occurred during the plating operation and was not relieved subsequently as required.","PeriodicalId":294593,"journal":{"name":"ASM Failure Analysis Case Histories: Processing Errors and Defects","volume":"16 1","pages":"0"},"PeriodicalIF":0.0,"publicationDate":"2019-06-01","publicationTypes":"Journal Article","fieldsOfStudy":null,"isOpenAccess":false,"openAccessPdf":"","citationCount":null,"resultStr":null,"platform":"Semanticscholar","paperid":"132044039","PeriodicalName":null,"FirstCategoryId":null,"ListUrlMain":null,"RegionNum":0,"RegionCategory":"","ArticlePicture":[],"TitleCN":null,"AbstractTextCN":null,"PMCID":"","EPubDate":null,"PubModel":null,"JCR":null,"JCRName":null,"Score":null,"Total":0}
Pub Date : 2019-06-01DOI: 10.31399/asm.fach.process.c9001425
An 850 ft. long steam main working at a pressure of 120 psi ruptured. Two lengths of pipe were submitted for examination, one containing the rupture and the other from an unaffected part removed to facilitate repair. The rupture surfaces were smooth, suggesting that the failure had taken place either at a weld in the pipe or at a discontinuity in the material. Microscopic examination through the joints at the ends of the rupture confirmed that the pipe had been made from strip and the edges lap-welded. The second case concerned an 8 in. diam pipe in which a longitudinal defect was discovered running the entire length. Examination of a section through the pipe containing the defect, showed this to be a scarf-welded pipe, only about half the section of the scarf having been satisfactorily welded together. It was concluded that both pipes had been defective at the time of manufacture and that service conditions had served to extend the defects.
{"title":"Defective Scarf Welds in Steel Pipes","authors":"","doi":"10.31399/asm.fach.process.c9001425","DOIUrl":"https://doi.org/10.31399/asm.fach.process.c9001425","url":null,"abstract":"\u0000 An 850 ft. long steam main working at a pressure of 120 psi ruptured. Two lengths of pipe were submitted for examination, one containing the rupture and the other from an unaffected part removed to facilitate repair. The rupture surfaces were smooth, suggesting that the failure had taken place either at a weld in the pipe or at a discontinuity in the material. Microscopic examination through the joints at the ends of the rupture confirmed that the pipe had been made from strip and the edges lap-welded. The second case concerned an 8 in. diam pipe in which a longitudinal defect was discovered running the entire length. Examination of a section through the pipe containing the defect, showed this to be a scarf-welded pipe, only about half the section of the scarf having been satisfactorily welded together. It was concluded that both pipes had been defective at the time of manufacture and that service conditions had served to extend the defects.","PeriodicalId":294593,"journal":{"name":"ASM Failure Analysis Case Histories: Processing Errors and Defects","volume":"26 1","pages":"0"},"PeriodicalIF":0.0,"publicationDate":"2019-06-01","publicationTypes":"Journal Article","fieldsOfStudy":null,"isOpenAccess":false,"openAccessPdf":"","citationCount":null,"resultStr":null,"platform":"Semanticscholar","paperid":"134111332","PeriodicalName":null,"FirstCategoryId":null,"ListUrlMain":null,"RegionNum":0,"RegionCategory":"","ArticlePicture":[],"TitleCN":null,"AbstractTextCN":null,"PMCID":"","EPubDate":null,"PubModel":null,"JCR":null,"JCRName":null,"Score":null,"Total":0}
Pub Date : 2019-06-01DOI: 10.31399/asm.fach.process.c9001908
M. Pepi
Cluster bomb tailcone assemblies each containing two aluminum die-cast components were rejected because of the poor surface condition of the die castings. Numerous heat checks were found on the surfaces of the tailcones and radiographic inspection revealed inclusions, gas holes, and shrinkage defects in the castings. Most of the components failed to meet required mechanical properties because of these casting defects.
{"title":"Failure of Die Cast Aluminum Cluster Bomb Tailcone Assemblies","authors":"M. Pepi","doi":"10.31399/asm.fach.process.c9001908","DOIUrl":"https://doi.org/10.31399/asm.fach.process.c9001908","url":null,"abstract":"\u0000 Cluster bomb tailcone assemblies each containing two aluminum die-cast components were rejected because of the poor surface condition of the die castings. Numerous heat checks were found on the surfaces of the tailcones and radiographic inspection revealed inclusions, gas holes, and shrinkage defects in the castings. Most of the components failed to meet required mechanical properties because of these casting defects.","PeriodicalId":294593,"journal":{"name":"ASM Failure Analysis Case Histories: Processing Errors and Defects","volume":"1 1","pages":"0"},"PeriodicalIF":0.0,"publicationDate":"2019-06-01","publicationTypes":"Journal Article","fieldsOfStudy":null,"isOpenAccess":false,"openAccessPdf":"","citationCount":null,"resultStr":null,"platform":"Semanticscholar","paperid":"131157569","PeriodicalName":null,"FirstCategoryId":null,"ListUrlMain":null,"RegionNum":0,"RegionCategory":"","ArticlePicture":[],"TitleCN":null,"AbstractTextCN":null,"PMCID":"","EPubDate":null,"PubModel":null,"JCR":null,"JCRName":null,"Score":null,"Total":0}
Pub Date : 2019-06-01DOI: 10.31399/asm.fach.process.c9001641
D. Aliya
Near-surface porosity in zinc die castings that were subsequently plated with copper, nickel, and bright chromium was causing blemishes in the plating. Identifying die casting turbulence and hot spots were keys to process modifications that subsequently allowed porosity to be greatly minimized.
{"title":"Plating Blemishes in Zinc Die Castings","authors":"D. Aliya","doi":"10.31399/asm.fach.process.c9001641","DOIUrl":"https://doi.org/10.31399/asm.fach.process.c9001641","url":null,"abstract":"\u0000 Near-surface porosity in zinc die castings that were subsequently plated with copper, nickel, and bright chromium was causing blemishes in the plating. Identifying die casting turbulence and hot spots were keys to process modifications that subsequently allowed porosity to be greatly minimized.","PeriodicalId":294593,"journal":{"name":"ASM Failure Analysis Case Histories: Processing Errors and Defects","volume":"58 4","pages":"0"},"PeriodicalIF":0.0,"publicationDate":"2019-06-01","publicationTypes":"Journal Article","fieldsOfStudy":null,"isOpenAccess":false,"openAccessPdf":"","citationCount":null,"resultStr":null,"platform":"Semanticscholar","paperid":"114060304","PeriodicalName":null,"FirstCategoryId":null,"ListUrlMain":null,"RegionNum":0,"RegionCategory":"","ArticlePicture":[],"TitleCN":null,"AbstractTextCN":null,"PMCID":"","EPubDate":null,"PubModel":null,"JCR":null,"JCRName":null,"Score":null,"Total":0}
Pub Date : 2019-06-01DOI: 10.31399/asm.fach.process.c9001203
F. Naumann, F. Spies
Three bearing bosses from the cover of scrap shears were sent in for examination. They had torn off the base plate to which they had been welded by fillet welds all around. Two of these were examined. They showed entirely the same symptoms. The bosses had broken away on three sides along the welds. The cleaved fractures in the burned notches propagated partially above and partially below several incipient cracks which may have been fatigue fractures. Metallographic sections showed that the fractures had occurred either at the burned notches near the transition from the weld to the sheet, or else they ran in the sheet material next to the weld. The quality of the welds could not be judged because the opposite fracture pieces to which they adhered had not been sent in. It was concluded that the breakaway of these bosses was at least favored by overheating and hardening.
{"title":"Broken-Off Bearing Bosses of Scrap Shears","authors":"F. Naumann, F. Spies","doi":"10.31399/asm.fach.process.c9001203","DOIUrl":"https://doi.org/10.31399/asm.fach.process.c9001203","url":null,"abstract":"\u0000 Three bearing bosses from the cover of scrap shears were sent in for examination. They had torn off the base plate to which they had been welded by fillet welds all around. Two of these were examined. They showed entirely the same symptoms. The bosses had broken away on three sides along the welds. The cleaved fractures in the burned notches propagated partially above and partially below several incipient cracks which may have been fatigue fractures. Metallographic sections showed that the fractures had occurred either at the burned notches near the transition from the weld to the sheet, or else they ran in the sheet material next to the weld. The quality of the welds could not be judged because the opposite fracture pieces to which they adhered had not been sent in. It was concluded that the breakaway of these bosses was at least favored by overheating and hardening.","PeriodicalId":294593,"journal":{"name":"ASM Failure Analysis Case Histories: Processing Errors and Defects","volume":"107 1","pages":"0"},"PeriodicalIF":0.0,"publicationDate":"2019-06-01","publicationTypes":"Journal Article","fieldsOfStudy":null,"isOpenAccess":false,"openAccessPdf":"","citationCount":null,"resultStr":null,"platform":"Semanticscholar","paperid":"123811621","PeriodicalName":null,"FirstCategoryId":null,"ListUrlMain":null,"RegionNum":0,"RegionCategory":"","ArticlePicture":[],"TitleCN":null,"AbstractTextCN":null,"PMCID":"","EPubDate":null,"PubModel":null,"JCR":null,"JCRName":null,"Score":null,"Total":0}
Pub Date : 2019-06-01DOI: 10.31399/asm.fach.process.c0048156
A 6150 flat spring was found to be failed. The face of the spring was revealed to be under tensile stress. The failure was concluded to have begun at the dark spot on the edge where roughness resulted from shearing during the blanking operation.
{"title":"Flat-Spring Failure Due to an Edge Defect","authors":"","doi":"10.31399/asm.fach.process.c0048156","DOIUrl":"https://doi.org/10.31399/asm.fach.process.c0048156","url":null,"abstract":"\u0000 A 6150 flat spring was found to be failed. The face of the spring was revealed to be under tensile stress. The failure was concluded to have begun at the dark spot on the edge where roughness resulted from shearing during the blanking operation.","PeriodicalId":294593,"journal":{"name":"ASM Failure Analysis Case Histories: Processing Errors and Defects","volume":"42 1","pages":"0"},"PeriodicalIF":0.0,"publicationDate":"2019-06-01","publicationTypes":"Journal Article","fieldsOfStudy":null,"isOpenAccess":false,"openAccessPdf":"","citationCount":null,"resultStr":null,"platform":"Semanticscholar","paperid":"122438445","PeriodicalName":null,"FirstCategoryId":null,"ListUrlMain":null,"RegionNum":0,"RegionCategory":"","ArticlePicture":[],"TitleCN":null,"AbstractTextCN":null,"PMCID":"","EPubDate":null,"PubModel":null,"JCR":null,"JCRName":null,"Score":null,"Total":0}