首页 > 最新文献

ASM Failure Analysis Case Histories: Processing Errors and Defects最新文献

英文 中文
Surface Indications in Hot-Rolled 4130 Steel Bars 热轧4130钢棒的表面指示
Pub Date : 2019-06-01 DOI: 10.31399/asm.fach.process.c0047161
Routine magnetic-particle inspection revealed crack indications in a number of shafts produced from hot-rolled 4130 steel bar. A pronounced indication of this size is cause for rejection if the defect is not eliminated during subsequent machining. A microstructural analysis of the shaft cross section revealed that the crack was approximately 0.5 mm (0.020 in.) deep and oriented in a radial direction. Furthermore, no stringer-type nonmetallic inclusions were observed in the vicinity of the flaw, which did not display the intergranular characteristics of a quench crack. The defect did, however, contain substantial amounts of oxide, which evidently resulted from the hot-working operation. This evidence supports the conclusion that the appearance of this discontinuity, with the long axis parallel to the working direction and radial orientation with regard to depth, strongly suggests a seam produced during rolling. Use of components with surface-defect indications as small as 0.5 mm (0.02 in.) can be risky in certain circumstances. Depending on the orientation of the flaw with respect to applied loads, the nature of the applied forces (for example, cyclic), and the operating environment, such a surface flaw can become the initiating site for a fatigue crack or a corrosion-related failure.
常规磁粉检查发现,在热轧4130钢棒生产的一些轴上有裂纹迹象。如果在随后的加工中不消除缺陷,这个尺寸的明显指示将导致拒收。轴横截面的显微结构分析表明,裂纹深度约为0.5 mm(0.020英寸),并呈径向取向。此外,在裂纹附近没有观察到斯特林格型非金属夹杂物,这没有显示出淬火裂纹的晶间特征。然而,缺陷确实含有大量的氧化物,这显然是由热加工操作造成的。这一证据支持这样的结论,即这种与工作方向平行的长轴和与深度有关的径向方向的不连续的出现,强烈表明在轧制过程中产生了接缝。在某些情况下,使用表面缺陷指示小至0.5毫米(0.02英寸)的组件可能存在风险。根据缺陷的方向、施加力的性质(例如,循环)和操作环境的不同,这种表面缺陷可能成为疲劳裂纹或腐蚀相关失效的起始点。
{"title":"Surface Indications in Hot-Rolled 4130 Steel Bars","authors":"","doi":"10.31399/asm.fach.process.c0047161","DOIUrl":"https://doi.org/10.31399/asm.fach.process.c0047161","url":null,"abstract":"\u0000 Routine magnetic-particle inspection revealed crack indications in a number of shafts produced from hot-rolled 4130 steel bar. A pronounced indication of this size is cause for rejection if the defect is not eliminated during subsequent machining. A microstructural analysis of the shaft cross section revealed that the crack was approximately 0.5 mm (0.020 in.) deep and oriented in a radial direction. Furthermore, no stringer-type nonmetallic inclusions were observed in the vicinity of the flaw, which did not display the intergranular characteristics of a quench crack. The defect did, however, contain substantial amounts of oxide, which evidently resulted from the hot-working operation. This evidence supports the conclusion that the appearance of this discontinuity, with the long axis parallel to the working direction and radial orientation with regard to depth, strongly suggests a seam produced during rolling. Use of components with surface-defect indications as small as 0.5 mm (0.02 in.) can be risky in certain circumstances. Depending on the orientation of the flaw with respect to applied loads, the nature of the applied forces (for example, cyclic), and the operating environment, such a surface flaw can become the initiating site for a fatigue crack or a corrosion-related failure.","PeriodicalId":294593,"journal":{"name":"ASM Failure Analysis Case Histories: Processing Errors and Defects","volume":"135 1","pages":"0"},"PeriodicalIF":0.0,"publicationDate":"2019-06-01","publicationTypes":"Journal Article","fieldsOfStudy":null,"isOpenAccess":false,"openAccessPdf":"","citationCount":null,"resultStr":null,"platform":"Semanticscholar","paperid":"126273559","PeriodicalName":null,"FirstCategoryId":null,"ListUrlMain":null,"RegionNum":0,"RegionCategory":"","ArticlePicture":[],"TitleCN":null,"AbstractTextCN":null,"PMCID":"","EPubDate":null,"PubModel":null,"JCR":null,"JCRName":null,"Score":null,"Total":0}
引用次数: 0
Fatigue Fracture of Waspaloy Spray-Manifold Assembly Because of Embrittlement by Penetration of Molten Braze Metal 熔钎金属渗透脆化导致的沃斯帕洛合金喷涂歧管总成疲劳断裂
Pub Date : 2019-06-01 DOI: 10.31399/asm.fach.process.c0047756
Waspaloy (AMS 5586) fabricated inner ring of a spray-manifold assembly failed transversely through the manifold tubing at the edge of the tube and support sleeve brazed joint. The assembly was brazed with AWS BAu-4 filler metal (AMS 4787). Fatigue beach marks propagating from extremities of a granular gold-tinted surface region adjacent to the tube-to-sleeve brazed joint and extending circumferentially were revealed by microscopic examination. Embrittlement of the tube caused by molten braze metal penetration along grain boundaries was evidenced by micrographs of a granular portion of the fracture. It was revealed by the initial fracture profile that fatigue cracks begun as an intergranular separation and subsequently became transgranular. It was concluded that failure of the tube was caused by excessive alloying between the braze metal and the Waspaloy. Reduced temperatures during torch debrazing or rebrazing were recommended to minimize molten braze metal penetration.
沃斯帕洛伊(AMS 5586)制造的喷淋管汇组件的内环在管和支撑套钎焊接头的边缘横向穿过管汇管。该组件用AWS BAu-4填充金属(AMS 4787)钎焊。显微检查发现,疲劳滩痕迹从靠近管套钎焊接头的颗粒状金色表面区域的末端传播并向周向延伸。熔钎金属沿晶界渗透引起的管的脆化由断口的颗粒部分的显微照片证明。初始断裂剖面显示,疲劳裂纹以沿晶分离开始,随后转变为穿晶断裂。结果表明,管的失效是由于钎焊金属与瓦斯帕洛合金之间的过度合金化造成的。建议在火炬除钎焊或重钎焊期间降低温度,以尽量减少熔融钎焊金属的渗透。
{"title":"Fatigue Fracture of Waspaloy Spray-Manifold Assembly Because of Embrittlement by Penetration of Molten Braze Metal","authors":"","doi":"10.31399/asm.fach.process.c0047756","DOIUrl":"https://doi.org/10.31399/asm.fach.process.c0047756","url":null,"abstract":"\u0000 Waspaloy (AMS 5586) fabricated inner ring of a spray-manifold assembly failed transversely through the manifold tubing at the edge of the tube and support sleeve brazed joint. The assembly was brazed with AWS BAu-4 filler metal (AMS 4787). Fatigue beach marks propagating from extremities of a granular gold-tinted surface region adjacent to the tube-to-sleeve brazed joint and extending circumferentially were revealed by microscopic examination. Embrittlement of the tube caused by molten braze metal penetration along grain boundaries was evidenced by micrographs of a granular portion of the fracture. It was revealed by the initial fracture profile that fatigue cracks begun as an intergranular separation and subsequently became transgranular. It was concluded that failure of the tube was caused by excessive alloying between the braze metal and the Waspaloy. Reduced temperatures during torch debrazing or rebrazing were recommended to minimize molten braze metal penetration.","PeriodicalId":294593,"journal":{"name":"ASM Failure Analysis Case Histories: Processing Errors and Defects","volume":"214 1","pages":"0"},"PeriodicalIF":0.0,"publicationDate":"2019-06-01","publicationTypes":"Journal Article","fieldsOfStudy":null,"isOpenAccess":false,"openAccessPdf":"","citationCount":null,"resultStr":null,"platform":"Semanticscholar","paperid":"122376480","PeriodicalName":null,"FirstCategoryId":null,"ListUrlMain":null,"RegionNum":0,"RegionCategory":"","ArticlePicture":[],"TitleCN":null,"AbstractTextCN":null,"PMCID":"","EPubDate":null,"PubModel":null,"JCR":null,"JCRName":null,"Score":null,"Total":0}
引用次数: 0
Fatigue Failure Caused by Weld Spatter 焊接飞溅引起的疲劳失效
Pub Date : 2019-06-01 DOI: 10.31399/asm.fach.process.c0048154
A medium-carbon helical spring was installed in a machine assembly that was welded into its final location. Weld spatter was not prevented from landing on the wire surface by any shield. An elongated drop and two tiny droplets of metal were observed a short distance from the fracture. No droplets were revealed at the origin of the fracture, but it was assumed that a drop of molten metal landed at the origin. Adherence of the spatter drop was expected to have been affected by the opening and closing of the fatigue crack. Weld spatter bead was concluded to have caused the fatigue fracture.
一个中碳螺旋弹簧被安装在焊接到最终位置的机器组件中。焊接飞溅没有被任何护罩阻止落在金属丝表面。在离断口不远的地方观察到一个细长的液滴和两个微小的金属液滴。在断口处没有发现液滴,但假设有一滴熔融金属落在了断口处。预计飞溅液滴的粘附性受到疲劳裂纹的打开和关闭的影响。焊接飞溅珠是造成疲劳断裂的主要原因。
{"title":"Fatigue Failure Caused by Weld Spatter","authors":"","doi":"10.31399/asm.fach.process.c0048154","DOIUrl":"https://doi.org/10.31399/asm.fach.process.c0048154","url":null,"abstract":"\u0000 A medium-carbon helical spring was installed in a machine assembly that was welded into its final location. Weld spatter was not prevented from landing on the wire surface by any shield. An elongated drop and two tiny droplets of metal were observed a short distance from the fracture. No droplets were revealed at the origin of the fracture, but it was assumed that a drop of molten metal landed at the origin. Adherence of the spatter drop was expected to have been affected by the opening and closing of the fatigue crack. Weld spatter bead was concluded to have caused the fatigue fracture.","PeriodicalId":294593,"journal":{"name":"ASM Failure Analysis Case Histories: Processing Errors and Defects","volume":"7 1","pages":"0"},"PeriodicalIF":0.0,"publicationDate":"2019-06-01","publicationTypes":"Journal Article","fieldsOfStudy":null,"isOpenAccess":false,"openAccessPdf":"","citationCount":null,"resultStr":null,"platform":"Semanticscholar","paperid":"128112015","PeriodicalName":null,"FirstCategoryId":null,"ListUrlMain":null,"RegionNum":0,"RegionCategory":"","ArticlePicture":[],"TitleCN":null,"AbstractTextCN":null,"PMCID":"","EPubDate":null,"PubModel":null,"JCR":null,"JCRName":null,"Score":null,"Total":0}
引用次数: 0
Failure of Valve Spring Because of Grinding and Shot Peening Operations 由于研磨和喷丸处理导致气门弹簧失效
Pub Date : 2019-06-01 DOI: 10.31399/asm.fach.process.c0048124
Presence of transverse marks which were remnant of grinding was indicated in a failed valve spring made from ground rod. The shot-peening pattern was light at this location. A transverse crack was found to grow from one such mark under the influence of local stress fields until it was reoriented to the plane normal to the major tensile axis by sufficient loading. The shot-peening procedure was altered to create adequate surface compression at all stressed points on the springs.
用地棒制成的气门弹簧失效后,存在磨削残余的横向痕迹。喷丸的痕迹在这个地方很轻。发现横向裂纹在局部应力场的影响下从一个这样的标记生长,直到在足够的加载下重新定向到与主拉伸轴垂直的平面。喷丸程序被改变,以在弹簧的所有应力点上产生足够的表面压缩。
{"title":"Failure of Valve Spring Because of Grinding and Shot Peening Operations","authors":"","doi":"10.31399/asm.fach.process.c0048124","DOIUrl":"https://doi.org/10.31399/asm.fach.process.c0048124","url":null,"abstract":"\u0000 Presence of transverse marks which were remnant of grinding was indicated in a failed valve spring made from ground rod. The shot-peening pattern was light at this location. A transverse crack was found to grow from one such mark under the influence of local stress fields until it was reoriented to the plane normal to the major tensile axis by sufficient loading. The shot-peening procedure was altered to create adequate surface compression at all stressed points on the springs.","PeriodicalId":294593,"journal":{"name":"ASM Failure Analysis Case Histories: Processing Errors and Defects","volume":"16 1","pages":"0"},"PeriodicalIF":0.0,"publicationDate":"2019-06-01","publicationTypes":"Journal Article","fieldsOfStudy":null,"isOpenAccess":false,"openAccessPdf":"","citationCount":null,"resultStr":null,"platform":"Semanticscholar","paperid":"128485651","PeriodicalName":null,"FirstCategoryId":null,"ListUrlMain":null,"RegionNum":0,"RegionCategory":"","ArticlePicture":[],"TitleCN":null,"AbstractTextCN":null,"PMCID":"","EPubDate":null,"PubModel":null,"JCR":null,"JCRName":null,"Score":null,"Total":0}
引用次数: 0
Fracture of an Accumulator Ring Due to Hydrogen Embrittlement 氢脆导致蓄能器环断裂
Pub Date : 2019-06-01 DOI: 10.31399/asm.fach.process.c0047192
Fracture of a cadmium-plated accumulator ring forged from 4140 steel was discovered during inspection and disassembly of a hydraulic-accumulator system stored at a depot. The ring had broken into five small and two large segments. The small segments of the broken ring displayed very flat fracture surfaces with no apparent yielding, but the two large segments did show evidence of bending (yielding) near the fractures. In addition, some segments contained fine radial cracks. Analysis (visual inspection, optical microscopy on polished-and-etched specimens, hardness testing, and chemical analysis) supported the conclusion that the failure was caused due to brittle fatigue, as evidenced by the intergranular nature of the fracture path. Also, hydrogen penetration occurred during the plating operation and was not relieved subsequently as required.
在检查和拆卸储存在仓库的液压蓄能器系统时,发现用4140钢锻造的镀镉蓄能器环断裂。戒指碎成了五小两大块。断裂环的一小部分显示出非常平坦的断口表面,没有明显的屈服,但两个大的部分在断口附近确实显示出弯曲(屈服)的证据。此外,部分管片还存在细小的径向裂纹。分析(对抛光和蚀刻样品的目视检查、光学显微镜检查、硬度测试和化学分析)支持了断裂是由脆性疲劳引起的结论,这一点可以从断裂路径的晶间性质中得到证明。此外,在电镀过程中发生了氢渗透,随后没有按要求解除。
{"title":"Fracture of an Accumulator Ring Due to Hydrogen Embrittlement","authors":"","doi":"10.31399/asm.fach.process.c0047192","DOIUrl":"https://doi.org/10.31399/asm.fach.process.c0047192","url":null,"abstract":"\u0000 Fracture of a cadmium-plated accumulator ring forged from 4140 steel was discovered during inspection and disassembly of a hydraulic-accumulator system stored at a depot. The ring had broken into five small and two large segments. The small segments of the broken ring displayed very flat fracture surfaces with no apparent yielding, but the two large segments did show evidence of bending (yielding) near the fractures. In addition, some segments contained fine radial cracks. Analysis (visual inspection, optical microscopy on polished-and-etched specimens, hardness testing, and chemical analysis) supported the conclusion that the failure was caused due to brittle fatigue, as evidenced by the intergranular nature of the fracture path. Also, hydrogen penetration occurred during the plating operation and was not relieved subsequently as required.","PeriodicalId":294593,"journal":{"name":"ASM Failure Analysis Case Histories: Processing Errors and Defects","volume":"16 1","pages":"0"},"PeriodicalIF":0.0,"publicationDate":"2019-06-01","publicationTypes":"Journal Article","fieldsOfStudy":null,"isOpenAccess":false,"openAccessPdf":"","citationCount":null,"resultStr":null,"platform":"Semanticscholar","paperid":"132044039","PeriodicalName":null,"FirstCategoryId":null,"ListUrlMain":null,"RegionNum":0,"RegionCategory":"","ArticlePicture":[],"TitleCN":null,"AbstractTextCN":null,"PMCID":"","EPubDate":null,"PubModel":null,"JCR":null,"JCRName":null,"Score":null,"Total":0}
引用次数: 0
Defective Scarf Welds in Steel Pipes 钢管围焊处有缺陷
Pub Date : 2019-06-01 DOI: 10.31399/asm.fach.process.c9001425
An 850 ft. long steam main working at a pressure of 120 psi ruptured. Two lengths of pipe were submitted for examination, one containing the rupture and the other from an unaffected part removed to facilitate repair. The rupture surfaces were smooth, suggesting that the failure had taken place either at a weld in the pipe or at a discontinuity in the material. Microscopic examination through the joints at the ends of the rupture confirmed that the pipe had been made from strip and the edges lap-welded. The second case concerned an 8 in. diam pipe in which a longitudinal defect was discovered running the entire length. Examination of a section through the pipe containing the defect, showed this to be a scarf-welded pipe, only about half the section of the scarf having been satisfactorily welded together. It was concluded that both pipes had been defective at the time of manufacture and that service conditions had served to extend the defects.
在120 psi压力下工作的850英尺长的蒸汽总管破裂。两段管道被提交检查,一段包含破裂,另一段来自未受影响的部分,以便于修复。破裂面很光滑,表明破裂发生在管道的焊缝或材料的不连续处。通过断口末端的接头进行显微检查,证实管子是用带钢制成的,边缘是搭接的。第二个案例涉及8英寸。直径管,其中纵向缺陷被发现贯穿整个长度。通过含有缺陷的管道的一段检查,表明这是一个围巾焊接管,只有大约一半的围巾部分已令人满意地焊接在一起。得出的结论是,这两根管子在制造时就有缺陷,使用条件延长了缺陷。
{"title":"Defective Scarf Welds in Steel Pipes","authors":"","doi":"10.31399/asm.fach.process.c9001425","DOIUrl":"https://doi.org/10.31399/asm.fach.process.c9001425","url":null,"abstract":"\u0000 An 850 ft. long steam main working at a pressure of 120 psi ruptured. Two lengths of pipe were submitted for examination, one containing the rupture and the other from an unaffected part removed to facilitate repair. The rupture surfaces were smooth, suggesting that the failure had taken place either at a weld in the pipe or at a discontinuity in the material. Microscopic examination through the joints at the ends of the rupture confirmed that the pipe had been made from strip and the edges lap-welded. The second case concerned an 8 in. diam pipe in which a longitudinal defect was discovered running the entire length. Examination of a section through the pipe containing the defect, showed this to be a scarf-welded pipe, only about half the section of the scarf having been satisfactorily welded together. It was concluded that both pipes had been defective at the time of manufacture and that service conditions had served to extend the defects.","PeriodicalId":294593,"journal":{"name":"ASM Failure Analysis Case Histories: Processing Errors and Defects","volume":"26 1","pages":"0"},"PeriodicalIF":0.0,"publicationDate":"2019-06-01","publicationTypes":"Journal Article","fieldsOfStudy":null,"isOpenAccess":false,"openAccessPdf":"","citationCount":null,"resultStr":null,"platform":"Semanticscholar","paperid":"134111332","PeriodicalName":null,"FirstCategoryId":null,"ListUrlMain":null,"RegionNum":0,"RegionCategory":"","ArticlePicture":[],"TitleCN":null,"AbstractTextCN":null,"PMCID":"","EPubDate":null,"PubModel":null,"JCR":null,"JCRName":null,"Score":null,"Total":0}
引用次数: 0
Failure of Die Cast Aluminum Cluster Bomb Tailcone Assemblies 压铸铝集束炸弹尾锥组件失效
Pub Date : 2019-06-01 DOI: 10.31399/asm.fach.process.c9001908
M. Pepi
Cluster bomb tailcone assemblies each containing two aluminum die-cast components were rejected because of the poor surface condition of the die castings. Numerous heat checks were found on the surfaces of the tailcones and radiographic inspection revealed inclusions, gas holes, and shrinkage defects in the castings. Most of the components failed to meet required mechanical properties because of these casting defects.
由于压铸件的表面状况不佳,每个包含两个铝压铸部件的集束炸弹尾锥总成被拒绝。在尾锥表面进行了多次热检查,射线照相检查发现铸件中有夹杂物、气孔和收缩缺陷。由于这些铸造缺陷,大多数部件不能满足要求的机械性能。
{"title":"Failure of Die Cast Aluminum Cluster Bomb Tailcone Assemblies","authors":"M. Pepi","doi":"10.31399/asm.fach.process.c9001908","DOIUrl":"https://doi.org/10.31399/asm.fach.process.c9001908","url":null,"abstract":"\u0000 Cluster bomb tailcone assemblies each containing two aluminum die-cast components were rejected because of the poor surface condition of the die castings. Numerous heat checks were found on the surfaces of the tailcones and radiographic inspection revealed inclusions, gas holes, and shrinkage defects in the castings. Most of the components failed to meet required mechanical properties because of these casting defects.","PeriodicalId":294593,"journal":{"name":"ASM Failure Analysis Case Histories: Processing Errors and Defects","volume":"1 1","pages":"0"},"PeriodicalIF":0.0,"publicationDate":"2019-06-01","publicationTypes":"Journal Article","fieldsOfStudy":null,"isOpenAccess":false,"openAccessPdf":"","citationCount":null,"resultStr":null,"platform":"Semanticscholar","paperid":"131157569","PeriodicalName":null,"FirstCategoryId":null,"ListUrlMain":null,"RegionNum":0,"RegionCategory":"","ArticlePicture":[],"TitleCN":null,"AbstractTextCN":null,"PMCID":"","EPubDate":null,"PubModel":null,"JCR":null,"JCRName":null,"Score":null,"Total":0}
引用次数: 0
Plating Blemishes in Zinc Die Castings 锌压铸件的镀层缺陷
Pub Date : 2019-06-01 DOI: 10.31399/asm.fach.process.c9001641
D. Aliya
Near-surface porosity in zinc die castings that were subsequently plated with copper, nickel, and bright chromium was causing blemishes in the plating. Identifying die casting turbulence and hot spots were keys to process modifications that subsequently allowed porosity to be greatly minimized.
锌压铸件在随后镀上铜、镍和亮铬后,其近表面气孔导致镀层出现瑕疵。确定压铸湍流和热点是工艺改进的关键,从而使气孔率大大降低。
{"title":"Plating Blemishes in Zinc Die Castings","authors":"D. Aliya","doi":"10.31399/asm.fach.process.c9001641","DOIUrl":"https://doi.org/10.31399/asm.fach.process.c9001641","url":null,"abstract":"\u0000 Near-surface porosity in zinc die castings that were subsequently plated with copper, nickel, and bright chromium was causing blemishes in the plating. Identifying die casting turbulence and hot spots were keys to process modifications that subsequently allowed porosity to be greatly minimized.","PeriodicalId":294593,"journal":{"name":"ASM Failure Analysis Case Histories: Processing Errors and Defects","volume":"58 4","pages":"0"},"PeriodicalIF":0.0,"publicationDate":"2019-06-01","publicationTypes":"Journal Article","fieldsOfStudy":null,"isOpenAccess":false,"openAccessPdf":"","citationCount":null,"resultStr":null,"platform":"Semanticscholar","paperid":"114060304","PeriodicalName":null,"FirstCategoryId":null,"ListUrlMain":null,"RegionNum":0,"RegionCategory":"","ArticlePicture":[],"TitleCN":null,"AbstractTextCN":null,"PMCID":"","EPubDate":null,"PubModel":null,"JCR":null,"JCRName":null,"Score":null,"Total":0}
引用次数: 0
Broken-Off Bearing Bosses of Scrap Shears 废柴剪断轴承座
Pub Date : 2019-06-01 DOI: 10.31399/asm.fach.process.c9001203
F. Naumann, F. Spies
Three bearing bosses from the cover of scrap shears were sent in for examination. They had torn off the base plate to which they had been welded by fillet welds all around. Two of these were examined. They showed entirely the same symptoms. The bosses had broken away on three sides along the welds. The cleaved fractures in the burned notches propagated partially above and partially below several incipient cracks which may have been fatigue fractures. Metallographic sections showed that the fractures had occurred either at the burned notches near the transition from the weld to the sheet, or else they ran in the sheet material next to the weld. The quality of the welds could not be judged because the opposite fracture pieces to which they adhered had not been sent in. It was concluded that the breakaway of these bosses was at least favored by overheating and hardening.
剪板机盖上的三个轴承座被送去检查。他们把周围用角焊缝焊接的底板撕掉了。对其中两个进行了检查。他们表现出完全相同的症状钢圈沿焊缝有三面断裂。烧痕处的劈裂断口部分在几个可能为疲劳断口的初始裂纹上方和下方扩展。金相切片显示,断裂要么发生在焊缝到板材过渡处附近的烧痕处,要么发生在靠近焊缝的板材中。焊缝的质量无法判断,因为它们所粘附的相反的断口没有送进去。得出的结论是,这些boss的分离至少有利于过热和硬化。
{"title":"Broken-Off Bearing Bosses of Scrap Shears","authors":"F. Naumann, F. Spies","doi":"10.31399/asm.fach.process.c9001203","DOIUrl":"https://doi.org/10.31399/asm.fach.process.c9001203","url":null,"abstract":"\u0000 Three bearing bosses from the cover of scrap shears were sent in for examination. They had torn off the base plate to which they had been welded by fillet welds all around. Two of these were examined. They showed entirely the same symptoms. The bosses had broken away on three sides along the welds. The cleaved fractures in the burned notches propagated partially above and partially below several incipient cracks which may have been fatigue fractures. Metallographic sections showed that the fractures had occurred either at the burned notches near the transition from the weld to the sheet, or else they ran in the sheet material next to the weld. The quality of the welds could not be judged because the opposite fracture pieces to which they adhered had not been sent in. It was concluded that the breakaway of these bosses was at least favored by overheating and hardening.","PeriodicalId":294593,"journal":{"name":"ASM Failure Analysis Case Histories: Processing Errors and Defects","volume":"107 1","pages":"0"},"PeriodicalIF":0.0,"publicationDate":"2019-06-01","publicationTypes":"Journal Article","fieldsOfStudy":null,"isOpenAccess":false,"openAccessPdf":"","citationCount":null,"resultStr":null,"platform":"Semanticscholar","paperid":"123811621","PeriodicalName":null,"FirstCategoryId":null,"ListUrlMain":null,"RegionNum":0,"RegionCategory":"","ArticlePicture":[],"TitleCN":null,"AbstractTextCN":null,"PMCID":"","EPubDate":null,"PubModel":null,"JCR":null,"JCRName":null,"Score":null,"Total":0}
引用次数: 0
Flat-Spring Failure Due to an Edge Defect 由于边缘缺陷导致的平簧失效
Pub Date : 2019-06-01 DOI: 10.31399/asm.fach.process.c0048156
A 6150 flat spring was found to be failed. The face of the spring was revealed to be under tensile stress. The failure was concluded to have begun at the dark spot on the edge where roughness resulted from shearing during the blanking operation.
发现6150扁平弹簧失效。弹簧的表面显示出受到拉应力的作用。失败的结论是,已经开始在黑暗的点上的边缘,粗糙造成的剪切在落料操作。
{"title":"Flat-Spring Failure Due to an Edge Defect","authors":"","doi":"10.31399/asm.fach.process.c0048156","DOIUrl":"https://doi.org/10.31399/asm.fach.process.c0048156","url":null,"abstract":"\u0000 A 6150 flat spring was found to be failed. The face of the spring was revealed to be under tensile stress. The failure was concluded to have begun at the dark spot on the edge where roughness resulted from shearing during the blanking operation.","PeriodicalId":294593,"journal":{"name":"ASM Failure Analysis Case Histories: Processing Errors and Defects","volume":"42 1","pages":"0"},"PeriodicalIF":0.0,"publicationDate":"2019-06-01","publicationTypes":"Journal Article","fieldsOfStudy":null,"isOpenAccess":false,"openAccessPdf":"","citationCount":null,"resultStr":null,"platform":"Semanticscholar","paperid":"122438445","PeriodicalName":null,"FirstCategoryId":null,"ListUrlMain":null,"RegionNum":0,"RegionCategory":"","ArticlePicture":[],"TitleCN":null,"AbstractTextCN":null,"PMCID":"","EPubDate":null,"PubModel":null,"JCR":null,"JCRName":null,"Score":null,"Total":0}
引用次数: 0
期刊
ASM Failure Analysis Case Histories: Processing Errors and Defects
全部 Acc. Chem. Res. ACS Applied Bio Materials ACS Appl. Electron. Mater. ACS Appl. Energy Mater. ACS Appl. Mater. Interfaces ACS Appl. Nano Mater. ACS Appl. Polym. Mater. ACS BIOMATER-SCI ENG ACS Catal. ACS Cent. Sci. ACS Chem. Biol. ACS Chemical Health & Safety ACS Chem. Neurosci. ACS Comb. Sci. ACS Earth Space Chem. ACS Energy Lett. ACS Infect. Dis. ACS Macro Lett. ACS Mater. Lett. ACS Med. Chem. Lett. ACS Nano ACS Omega ACS Photonics ACS Sens. ACS Sustainable Chem. Eng. ACS Synth. Biol. Anal. Chem. BIOCHEMISTRY-US Bioconjugate Chem. BIOMACROMOLECULES Chem. Res. Toxicol. Chem. Rev. Chem. Mater. CRYST GROWTH DES ENERG FUEL Environ. Sci. Technol. Environ. Sci. Technol. Lett. Eur. J. Inorg. Chem. IND ENG CHEM RES Inorg. Chem. J. Agric. Food. Chem. J. Chem. Eng. Data J. Chem. Educ. J. Chem. Inf. Model. J. Chem. Theory Comput. J. Med. Chem. J. Nat. Prod. J PROTEOME RES J. Am. Chem. Soc. LANGMUIR MACROMOLECULES Mol. Pharmaceutics Nano Lett. Org. Lett. ORG PROCESS RES DEV ORGANOMETALLICS J. Org. Chem. J. Phys. Chem. J. Phys. Chem. A J. Phys. Chem. B J. Phys. Chem. C J. Phys. Chem. Lett. Analyst Anal. Methods Biomater. Sci. Catal. Sci. Technol. Chem. Commun. Chem. Soc. Rev. CHEM EDUC RES PRACT CRYSTENGCOMM Dalton Trans. Energy Environ. Sci. ENVIRON SCI-NANO ENVIRON SCI-PROC IMP ENVIRON SCI-WAT RES Faraday Discuss. Food Funct. Green Chem. Inorg. Chem. Front. Integr. Biol. J. Anal. At. Spectrom. J. Mater. Chem. A J. Mater. Chem. B J. Mater. Chem. C Lab Chip Mater. Chem. Front. Mater. Horiz. MEDCHEMCOMM Metallomics Mol. Biosyst. Mol. Syst. Des. Eng. Nanoscale Nanoscale Horiz. Nat. Prod. Rep. New J. Chem. Org. Biomol. Chem. Org. Chem. Front. PHOTOCH PHOTOBIO SCI PCCP Polym. Chem.
×
引用
GB/T 7714-2015
复制
MLA
复制
APA
复制
导出至
BibTeX EndNote RefMan NoteFirst NoteExpress
×
0
微信
客服QQ
Book学术公众号 扫码关注我们
反馈
×
意见反馈
请填写您的意见或建议
请填写您的手机或邮箱
×
提示
您的信息不完整,为了账户安全,请先补充。
现在去补充
×
提示
您因"违规操作"
具体请查看互助需知
我知道了
×
提示
现在去查看 取消
×
提示
确定
Book学术官方微信
Book学术文献互助
Book学术文献互助群
群 号:481959085
Book学术
文献互助 智能选刊 最新文献 互助须知 联系我们:info@booksci.cn
Book学术提供免费学术资源搜索服务,方便国内外学者检索中英文文献。致力于提供最便捷和优质的服务体验。
Copyright © 2023 Book学术 All rights reserved.
ghs 京公网安备 11010802042870号 京ICP备2023020795号-1