首页 > 最新文献

ASM Failure Analysis Case Histories: Processing Errors and Defects最新文献

英文 中文
Some Manufacturing Defects in Copper Conductors 铜导体的一些制造缺陷
Pub Date : 2019-06-01 DOI: 10.31399/asm.fach.process.c9001443
Following the fusing of one of the copper leads in the choke circuit of an electric welder, a piece of the affected lead was obtained for examination. The sample had large internal cavities and surface bulges. It is remarkable that a wire containing defects of the magnitude present in this case could have been drawn without failure. Failure in service was due to overheating resulting from the inability of the conductor to carry the current where its cross section was reduced by the presence of a cavity. Another failure of a conductor occurred in one of the field coils of a direct-current motor. The mode of failure and the changes in the microstructure showed that fracture was due to a defective resistance butt-weld which had been made when the wire was in process of drawing. A further example of a conductor failure occurred in a 12 SWG copper connection between the rotor contactor and the resistance in a starter. A transverse section through the zone of failure showed an oxide layer extended almost completely across the plane of a weld, and also the grain growth that had occurred in this region.
在电焊机扼流圈中的一根铜引线熔断后,取一块受影响的引线进行检查。样品有很大的内部空腔和表面凸起。值得注意的是,在这种情况下,含有如此严重缺陷的金属丝是可以毫无故障地拉出来的。在使用中失败是由于过热造成的,这是由于导体无法携带电流,而其横截面由于空腔的存在而减小。另一个导体故障发生在直流电机的一个磁场线圈中。失效模式和显微组织的变化表明,断裂是由于在拉丝过程中形成的电阻对接焊缝缺陷造成的。导体故障的另一个例子发生在转子接触器和起动器电阻之间的12 SWG铜连接中。通过破坏区域的横切面可以看到氧化层几乎完全延伸到焊缝平面上,并且在该区域也发生了晶粒生长。
{"title":"Some Manufacturing Defects in Copper Conductors","authors":"","doi":"10.31399/asm.fach.process.c9001443","DOIUrl":"https://doi.org/10.31399/asm.fach.process.c9001443","url":null,"abstract":"\u0000 Following the fusing of one of the copper leads in the choke circuit of an electric welder, a piece of the affected lead was obtained for examination. The sample had large internal cavities and surface bulges. It is remarkable that a wire containing defects of the magnitude present in this case could have been drawn without failure. Failure in service was due to overheating resulting from the inability of the conductor to carry the current where its cross section was reduced by the presence of a cavity. Another failure of a conductor occurred in one of the field coils of a direct-current motor. The mode of failure and the changes in the microstructure showed that fracture was due to a defective resistance butt-weld which had been made when the wire was in process of drawing. A further example of a conductor failure occurred in a 12 SWG copper connection between the rotor contactor and the resistance in a starter. A transverse section through the zone of failure showed an oxide layer extended almost completely across the plane of a weld, and also the grain growth that had occurred in this region.","PeriodicalId":294593,"journal":{"name":"ASM Failure Analysis Case Histories: Processing Errors and Defects","volume":"1 1","pages":"0"},"PeriodicalIF":0.0,"publicationDate":"2019-06-01","publicationTypes":"Journal Article","fieldsOfStudy":null,"isOpenAccess":false,"openAccessPdf":"","citationCount":null,"resultStr":null,"platform":"Semanticscholar","paperid":"130917167","PeriodicalName":null,"FirstCategoryId":null,"ListUrlMain":null,"RegionNum":0,"RegionCategory":"","ArticlePicture":[],"TitleCN":null,"AbstractTextCN":null,"PMCID":"","EPubDate":null,"PubModel":null,"JCR":null,"JCRName":null,"Score":null,"Total":0}
引用次数: 0
Fatigue Fracture of a 4140 Steel Forged Crankshaft Resulting From Stress Raisers Created During Hot Trimming 热切边过程中产生的应力引起的4140钢锻造曲轴疲劳断裂
Pub Date : 2019-06-01 DOI: 10.31399/asm.fach.process.c0047830
Textile-machine crankshafts forged from 4140 steel fractured transversely on one cheek during one to three years of service. The cause of failure for two forgings (one complete fractured forging and second a section that contained the shorter shaft fracture cheek) was determined. Indication of fatigue failure was revealed by visual examination of the fracture surfaces. Rough grooves from hot trimming of the flash were visible on the surface of the cheeks. The outer face of one cheek of the throw on the forging contained shallow surface folds. Slightly decarburized forged surface was identified around one of the folds and a fatigue crack initiated in the fold and propagated across the cheek. Properties representative of 4140 steel, quenched and tempered to a hardness of 20 to 22 HRC, were observed. Tempered bainite was revealed in the general microstructure. As a corrective measure, the forgings were normalized, hardened and tempered to 28 to 32 HRC before being machined to increase fatigue strength and extremely rough surfaces were removed by careful grinding.
4140钢锻造的纺织机曲轴在一到三年的使用期间在一个侧面横向断裂。确定了两个锻件的失效原因(一个锻件完全断裂,另一个锻件包含较短的轴断裂面)。断口表面的目视检查显示了疲劳失效的迹象。在脸颊的表面上可以看到闪光热修剪的粗糙凹槽。锻件上铸件的一个侧面的外表面有浅的表面褶皱。在其中一个褶皱周围发现了轻度脱碳的锻件表面,并且在褶皱处产生了疲劳裂纹并沿脸颊扩展。观察了具有代表性的4140钢的性能,淬火和回火的硬度为20至22 HRC。总体组织呈现回火贝氏体。作为一项纠正措施,锻件在加工前经过正火、淬火和回火至28至32 HRC,以提高疲劳强度,并通过仔细磨削去除极其粗糙的表面。
{"title":"Fatigue Fracture of a 4140 Steel Forged Crankshaft Resulting From Stress Raisers Created During Hot Trimming","authors":"","doi":"10.31399/asm.fach.process.c0047830","DOIUrl":"https://doi.org/10.31399/asm.fach.process.c0047830","url":null,"abstract":"\u0000 Textile-machine crankshafts forged from 4140 steel fractured transversely on one cheek during one to three years of service. The cause of failure for two forgings (one complete fractured forging and second a section that contained the shorter shaft fracture cheek) was determined. Indication of fatigue failure was revealed by visual examination of the fracture surfaces. Rough grooves from hot trimming of the flash were visible on the surface of the cheeks. The outer face of one cheek of the throw on the forging contained shallow surface folds. Slightly decarburized forged surface was identified around one of the folds and a fatigue crack initiated in the fold and propagated across the cheek. Properties representative of 4140 steel, quenched and tempered to a hardness of 20 to 22 HRC, were observed. Tempered bainite was revealed in the general microstructure. As a corrective measure, the forgings were normalized, hardened and tempered to 28 to 32 HRC before being machined to increase fatigue strength and extremely rough surfaces were removed by careful grinding.","PeriodicalId":294593,"journal":{"name":"ASM Failure Analysis Case Histories: Processing Errors and Defects","volume":"68 1","pages":"0"},"PeriodicalIF":0.0,"publicationDate":"2019-06-01","publicationTypes":"Journal Article","fieldsOfStudy":null,"isOpenAccess":false,"openAccessPdf":"","citationCount":null,"resultStr":null,"platform":"Semanticscholar","paperid":"116201177","PeriodicalName":null,"FirstCategoryId":null,"ListUrlMain":null,"RegionNum":0,"RegionCategory":"","ArticlePicture":[],"TitleCN":null,"AbstractTextCN":null,"PMCID":"","EPubDate":null,"PubModel":null,"JCR":null,"JCRName":null,"Score":null,"Total":0}
引用次数: 0
Failure During Fabrication of an Armature Because of Lamellar Tearing 电枢制造过程中由于片层撕裂造成的失效
Pub Date : 2019-06-01 DOI: 10.31399/asm.fach.process.c0089793
During the final shop welding of a large armature for a direct-current motor (4475 kW, or 6000 hp), a loud bang was heard, and the welding operation stopped. When the weld was cold, nondestructive evaluation revealed a large crack adjacent to the root weld. Investigation showed the main crack had propagated parallel to the fusion boundary along the subcritical HAZ and was associated with long stringers of type II manganese sulfide (MnS) inclusions. This supported the conclusion that the weld failed by lamellar tearing as a result of the high rotational strain induced at the root of the weld caused by the weld design, weld sequence, and thermal effects. Recommendations included removing the old weldment to a depth beyond the crack and replacing this with a softer weld metal layer before making the main weld onto the softer layer.
在对直流电机(4475千瓦或6000马力)的大型电枢进行最后一次车间焊接时,听到一声巨响,焊接工作停止了。当焊缝处于冷态时,无损评价显示根部焊缝附近有一个大裂纹。研究表明,主裂纹沿亚临界热影响区平行于熔合边界扩展,并伴有II型硫化锰(MnS)夹杂物的长串。这支持了以下结论:由于焊缝设计、焊接顺序和热效应在焊缝根部引起的高旋转应变,导致了焊缝的片层撕裂。建议包括将旧焊件移至裂纹以外的深度,并用较软的焊接金属层代替,然后再将主焊缝焊接到较软的金属层上。
{"title":"Failure During Fabrication of an Armature Because of Lamellar Tearing","authors":"","doi":"10.31399/asm.fach.process.c0089793","DOIUrl":"https://doi.org/10.31399/asm.fach.process.c0089793","url":null,"abstract":"\u0000 During the final shop welding of a large armature for a direct-current motor (4475 kW, or 6000 hp), a loud bang was heard, and the welding operation stopped. When the weld was cold, nondestructive evaluation revealed a large crack adjacent to the root weld. Investigation showed the main crack had propagated parallel to the fusion boundary along the subcritical HAZ and was associated with long stringers of type II manganese sulfide (MnS) inclusions. This supported the conclusion that the weld failed by lamellar tearing as a result of the high rotational strain induced at the root of the weld caused by the weld design, weld sequence, and thermal effects. Recommendations included removing the old weldment to a depth beyond the crack and replacing this with a softer weld metal layer before making the main weld onto the softer layer.","PeriodicalId":294593,"journal":{"name":"ASM Failure Analysis Case Histories: Processing Errors and Defects","volume":"56 1","pages":"0"},"PeriodicalIF":0.0,"publicationDate":"2019-06-01","publicationTypes":"Journal Article","fieldsOfStudy":null,"isOpenAccess":false,"openAccessPdf":"","citationCount":null,"resultStr":null,"platform":"Semanticscholar","paperid":"116296211","PeriodicalName":null,"FirstCategoryId":null,"ListUrlMain":null,"RegionNum":0,"RegionCategory":"","ArticlePicture":[],"TitleCN":null,"AbstractTextCN":null,"PMCID":"","EPubDate":null,"PubModel":null,"JCR":null,"JCRName":null,"Score":null,"Total":0}
引用次数: 0
Fatigue Fracture of a Carbon Steel Wiper Spring Because of Stress Concentration at a Sharp Corner 碳钢雨刮器弹簧尖角应力集中导致疲劳断裂
Pub Date : 2019-06-01 DOI: 10.31399/asm.fach.process.c0048150
Grease-wiper springs for cams formed from stampings of 0.25-mm thick carbon spring steel (0.65 to 0.80% C) fractured at the 0.025 mm radius on the stamped 135 deg corner at a 90 deg bend after 5,000,000 cycles. Tool marks 2 to 2.3 mm from the center of the stamped bend were disclosed by visual examination. Fatigue striations originating from cracks at the 0.025 mm radius inside corner at the bend were revealed by SEM of the fractured surface. The maximum stress at the bend, in stock of maximum thickness and as a function of the radius of the 135 deg corner, was indicated by stress calculations to be very close to the maximum allowable fluctuating stress for the material. The wiper springs were concluded to be fractured in fatigue and the cyclic loading resulted from cam rotation. The maximum applied stress approached the allowable limit due to high stress-concentration factor in the spring (caused by the very small inside radius). The corner radius was increased to 0.76 mm and the tools were re-polished to avoid tool marks.
由0.25毫米厚碳素弹簧钢(0.65至0.80% C)冲压而成的凸轮刮油器弹簧,在经过500万次循环后,在90度弯曲处的135度角上,在0.025毫米半径处断裂。从冲压弯管中心2到2.3毫米的工具标记通过目视检查被发现。断裂表面扫描电镜显示,弯曲处0.025 mm半径内角处的裂纹产生疲劳条纹。在弯曲处的最大应力,在最大厚度的库存和作为135度角半径的函数,应力计算表明,非常接近材料的最大允许波动应力。分析认为雨刷弹簧在疲劳和凸轮旋转的循环载荷作用下发生断裂。由于弹簧的应力集中系数高(由很小的内半径引起),最大施加应力接近允许极限。将转角半径增加到0.76 mm,并重新抛光刀具以避免刀痕。
{"title":"Fatigue Fracture of a Carbon Steel Wiper Spring Because of Stress Concentration at a Sharp Corner","authors":"","doi":"10.31399/asm.fach.process.c0048150","DOIUrl":"https://doi.org/10.31399/asm.fach.process.c0048150","url":null,"abstract":"\u0000 Grease-wiper springs for cams formed from stampings of 0.25-mm thick carbon spring steel (0.65 to 0.80% C) fractured at the 0.025 mm radius on the stamped 135 deg corner at a 90 deg bend after 5,000,000 cycles. Tool marks 2 to 2.3 mm from the center of the stamped bend were disclosed by visual examination. Fatigue striations originating from cracks at the 0.025 mm radius inside corner at the bend were revealed by SEM of the fractured surface. The maximum stress at the bend, in stock of maximum thickness and as a function of the radius of the 135 deg corner, was indicated by stress calculations to be very close to the maximum allowable fluctuating stress for the material. The wiper springs were concluded to be fractured in fatigue and the cyclic loading resulted from cam rotation. The maximum applied stress approached the allowable limit due to high stress-concentration factor in the spring (caused by the very small inside radius). The corner radius was increased to 0.76 mm and the tools were re-polished to avoid tool marks.","PeriodicalId":294593,"journal":{"name":"ASM Failure Analysis Case Histories: Processing Errors and Defects","volume":"15 1","pages":"0"},"PeriodicalIF":0.0,"publicationDate":"2019-06-01","publicationTypes":"Journal Article","fieldsOfStudy":null,"isOpenAccess":false,"openAccessPdf":"","citationCount":null,"resultStr":null,"platform":"Semanticscholar","paperid":"127862399","PeriodicalName":null,"FirstCategoryId":null,"ListUrlMain":null,"RegionNum":0,"RegionCategory":"","ArticlePicture":[],"TitleCN":null,"AbstractTextCN":null,"PMCID":"","EPubDate":null,"PubModel":null,"JCR":null,"JCRName":null,"Score":null,"Total":0}
引用次数: 0
Failure of a Welded Boiler Tube During a Bending Operation 焊接锅炉管在弯曲操作过程中的失效
Pub Date : 2019-06-01 DOI: 10.31399/asm.fach.process.c9001433
On attempting to manipulate or bend a boiler tube some 22 ft. long, sudden failure occurred at what appeared to be a butt weld in the tube. Externally, the weld reinforcement had been ground flush and the entire tube surface painted. Internally, the appearance and width of the heated band suggested that the weld had been made by the oxy-gas process. A lack of root fusion over most of its length was evident. Examination of the fracture faces, which were of crystalline appearance indicative of brittle behavior, indicated incomplete fusion of the weld root. Microscopic examination showed the deposit to possess a large grain size with a low carbon content disposed as carbides along the grain boundaries, a feature which would provide an explanation of the brittle behavior. Subsequent inspection showed that this tube was one of several of the batch ordered for retubing of a boiler and which had a 2 ft. length welded to one end to make up the length.
在试图操纵或弯曲约22英尺长的锅炉管时,突然发生故障,似乎是管中的对接焊缝。在外部,焊接加固已经地面平齐,整个管表面涂漆。在内部,加热带的外观和宽度表明焊接是由氧气工艺制成的。在它的大部分长度上缺乏根融合是明显的。断口表面呈结晶状,表明脆性行为,表明焊缝根部未完全融合。显微检查表明,该矿床具有大晶粒尺寸,低碳含量沿晶界以碳化物的形式分布,这一特征可以解释脆性行为。随后的检查表明,该管是为锅炉重新管道订购的几个批次之一,其中一端焊接有2英尺长,以弥补长度。
{"title":"Failure of a Welded Boiler Tube During a Bending Operation","authors":"","doi":"10.31399/asm.fach.process.c9001433","DOIUrl":"https://doi.org/10.31399/asm.fach.process.c9001433","url":null,"abstract":"\u0000 On attempting to manipulate or bend a boiler tube some 22 ft. long, sudden failure occurred at what appeared to be a butt weld in the tube. Externally, the weld reinforcement had been ground flush and the entire tube surface painted. Internally, the appearance and width of the heated band suggested that the weld had been made by the oxy-gas process. A lack of root fusion over most of its length was evident. Examination of the fracture faces, which were of crystalline appearance indicative of brittle behavior, indicated incomplete fusion of the weld root. Microscopic examination showed the deposit to possess a large grain size with a low carbon content disposed as carbides along the grain boundaries, a feature which would provide an explanation of the brittle behavior. Subsequent inspection showed that this tube was one of several of the batch ordered for retubing of a boiler and which had a 2 ft. length welded to one end to make up the length.","PeriodicalId":294593,"journal":{"name":"ASM Failure Analysis Case Histories: Processing Errors and Defects","volume":"106 1","pages":"0"},"PeriodicalIF":0.0,"publicationDate":"2019-06-01","publicationTypes":"Journal Article","fieldsOfStudy":null,"isOpenAccess":false,"openAccessPdf":"","citationCount":null,"resultStr":null,"platform":"Semanticscholar","paperid":"130445524","PeriodicalName":null,"FirstCategoryId":null,"ListUrlMain":null,"RegionNum":0,"RegionCategory":"","ArticlePicture":[],"TitleCN":null,"AbstractTextCN":null,"PMCID":"","EPubDate":null,"PubModel":null,"JCR":null,"JCRName":null,"Score":null,"Total":0}
引用次数: 0
Fracture of Welds in a Pressure Vessel Because of Atmospheric Contamination 压力容器中由于大气污染导致的焊缝断裂
Pub Date : 2019-06-01 DOI: 10.31399/asm.fach.process.c0047641
A Ti-6Al-4V alloy pressure vessel failed during a proof-pressure test, fracturing along the center girth weld. The girth joints were welded with the automatic gas tungsten arc process utilizing an auxiliary trailing shield attached to the welding torch to provide inert-gas shielding for the exterior surface of the weld. A segmented backup ring with a gas channel was used inside the vessel to shield the weld root. The pressure vessel failed due to contamination of the fusion zone by oxygen, which resulted when the gas shielding the root face of the weld was diluted by air that leaked into the gas channel. Thermal stresses cracked the embrittled weld, exposing the crack surfaces to oxidation before cooling. One of these cracks caused a stress concentration so severe that failure of the vessel wall during the proof test was inevitable. A sealing system at the split-line region of the segmented backup ring was provided, and a fine-mesh stainless steel screen diffuser was incorporated in the channel section of the backup ring to prevent air from leaking in. A titanium alloy color chart was furnished to permit correlation of weld-zone discoloration with the degree of atmospheric contamination.
Ti-6Al-4V合金压力容器在耐压测试中发生故障,沿中心环焊缝破裂。采用自动气体钨弧焊法焊接围接头,利用附在焊枪上的辅助尾随护罩为焊缝外表面提供惰性气体保护。在容器内使用带有气体通道的分段备份环来保护焊缝根部。由于氧气污染了熔合区,导致压力容器失效,这是由于保护焊缝根部表面的气体被泄漏到气体通道中的空气稀释所致。热应力使易碎的焊缝破裂,使裂纹表面在冷却前氧化。其中一个裂缝引起的应力集中如此严重,以致在证明试验中容器壁的破坏是不可避免的。在分段备份环的分割线区域设置了密封系统,在备份环的通道段设置了细孔不锈钢筛网扩散器,以防止空气泄漏。提供了钛合金颜色图,以便将焊接区变色与大气污染程度相关联。
{"title":"Fracture of Welds in a Pressure Vessel Because of Atmospheric Contamination","authors":"","doi":"10.31399/asm.fach.process.c0047641","DOIUrl":"https://doi.org/10.31399/asm.fach.process.c0047641","url":null,"abstract":"\u0000 A Ti-6Al-4V alloy pressure vessel failed during a proof-pressure test, fracturing along the center girth weld. The girth joints were welded with the automatic gas tungsten arc process utilizing an auxiliary trailing shield attached to the welding torch to provide inert-gas shielding for the exterior surface of the weld. A segmented backup ring with a gas channel was used inside the vessel to shield the weld root. The pressure vessel failed due to contamination of the fusion zone by oxygen, which resulted when the gas shielding the root face of the weld was diluted by air that leaked into the gas channel. Thermal stresses cracked the embrittled weld, exposing the crack surfaces to oxidation before cooling. One of these cracks caused a stress concentration so severe that failure of the vessel wall during the proof test was inevitable. A sealing system at the split-line region of the segmented backup ring was provided, and a fine-mesh stainless steel screen diffuser was incorporated in the channel section of the backup ring to prevent air from leaking in. A titanium alloy color chart was furnished to permit correlation of weld-zone discoloration with the degree of atmospheric contamination.","PeriodicalId":294593,"journal":{"name":"ASM Failure Analysis Case Histories: Processing Errors and Defects","volume":"90 1","pages":"0"},"PeriodicalIF":0.0,"publicationDate":"2019-06-01","publicationTypes":"Journal Article","fieldsOfStudy":null,"isOpenAccess":false,"openAccessPdf":"","citationCount":null,"resultStr":null,"platform":"Semanticscholar","paperid":"122839807","PeriodicalName":null,"FirstCategoryId":null,"ListUrlMain":null,"RegionNum":0,"RegionCategory":"","ArticlePicture":[],"TitleCN":null,"AbstractTextCN":null,"PMCID":"","EPubDate":null,"PubModel":null,"JCR":null,"JCRName":null,"Score":null,"Total":0}
引用次数: 0
Leaky Socket Pipe from the Safety Return Circuit of a Heating Installation 加热装置安全回路的承插管漏水
Pub Date : 2019-06-01 DOI: 10.31399/asm.fach.process.c9001211
Egon Kauczor
An elbow made from welded steel tube had become leaky along a well-defined line in the axial direction. The entire wall of the tube was corroded, and the longitudinally-welded seam stood out clearly as a result of particularly intensive corrosive attack. The appearance of the corroded surface indicates the action of water with a high oxygen content. The oxygen in the return water must have originated from the ventilation of the open expansion vessel. Because of the corrosion-favoring effect of a crevice, water with a high oxygen-content that was perhaps still warm or even hot found particularly favorable conditions for corrosion in the defective welded seam (crevice corrosion). The tube material itself is perfectly satisfactory and in no way responsible for the failure.
一个由焊接钢管制成的弯头在轴向沿一条明确的线发生了泄漏。整个管壁被腐蚀,纵向焊缝因腐蚀作用特别强烈而明显。腐蚀表面的外观表明高氧含量的水的作用。回水中的氧气一定是来自于打开的膨胀容器的通风。由于裂缝的腐蚀作用,含氧量高的水可能仍然是温暖的,甚至是热的,这对有缺陷的焊缝(裂缝腐蚀)的腐蚀特别有利。管材料本身是完全令人满意的,在任何方式负责的失败。
{"title":"Leaky Socket Pipe from the Safety Return Circuit of a Heating Installation","authors":"Egon Kauczor","doi":"10.31399/asm.fach.process.c9001211","DOIUrl":"https://doi.org/10.31399/asm.fach.process.c9001211","url":null,"abstract":"\u0000 An elbow made from welded steel tube had become leaky along a well-defined line in the axial direction. The entire wall of the tube was corroded, and the longitudinally-welded seam stood out clearly as a result of particularly intensive corrosive attack. The appearance of the corroded surface indicates the action of water with a high oxygen content. The oxygen in the return water must have originated from the ventilation of the open expansion vessel. Because of the corrosion-favoring effect of a crevice, water with a high oxygen-content that was perhaps still warm or even hot found particularly favorable conditions for corrosion in the defective welded seam (crevice corrosion). The tube material itself is perfectly satisfactory and in no way responsible for the failure.","PeriodicalId":294593,"journal":{"name":"ASM Failure Analysis Case Histories: Processing Errors and Defects","volume":"144 1","pages":"0"},"PeriodicalIF":0.0,"publicationDate":"2019-06-01","publicationTypes":"Journal Article","fieldsOfStudy":null,"isOpenAccess":false,"openAccessPdf":"","citationCount":null,"resultStr":null,"platform":"Semanticscholar","paperid":"124170342","PeriodicalName":null,"FirstCategoryId":null,"ListUrlMain":null,"RegionNum":0,"RegionCategory":"","ArticlePicture":[],"TitleCN":null,"AbstractTextCN":null,"PMCID":"","EPubDate":null,"PubModel":null,"JCR":null,"JCRName":null,"Score":null,"Total":0}
引用次数: 0
Failure by Blowout of Aluminum Alloy 6061-T6 Connector Tubes From a Water-Cooling System 水冷系统6061-T6铝合金接头管爆裂故障
Pub Date : 2019-06-01 DOI: 10.31399/asm.fach.process.c0047080
Several of the aluminum alloy 6061-T6 drawn seamless tubes (ASTM B 234, 2.5 cm (1.0 in.) OD with wall thickness of 1.7 mm (0.065 in.)) connecting an array of headers to a system of water-cooling pipes failed. The tubes were supplied in the O temper. They were bent to the desired curvature, preheated, then solution treated, water quenched, and then aged for 8 to 10 h. Analysis (visual inspection, slow-bend testing, 65x macrographic analysis, macroetching, spectrographic analysis, hardness tests, microhardness tests, tension tests, and microscopic examination) supported the conclusions that bending of the connector tubes in the annealed condition induced critical strain near the neutral axis of the tube, which resulted in excessive growth of individual grains during the subsequent solution treatment. Recommendations included bending the connector tubes in the T4 temper as early as possible after being quenched from the solution temperature. The tubes should be stored in dry ice after the quench until bending can be done. The tubes should be aged immediately after being formed. Flattening and slow-bend tests should be specified to ensure that the connector tubes had satisfactory ductility.
几种铝合金6061-T6拉伸无缝管(ASTM B 234, 2.5厘米(1.0英寸))外径为1.7毫米(0.065英寸),将一系列集管连接到水冷管系统失败。这些管子是用O型回火供应的。它们被弯曲到所需的曲率,预热,然后固溶处理,水淬火,然后老化8到10小时。分析(目测检查,慢弯曲测试,65倍宏观分析,宏观刻蚀,光谱分析,硬度测试,显微硬度测试,张力测试和显微检查)支持这样的结论,即在退火条件下连接器管的弯曲在管的中性轴附近引起临界应变。这导致在随后的固溶处理中单个晶粒过度生长。建议包括在从溶液温度淬火后尽早在T4回火中弯曲连接器管。淬火后,管子应保存在干冰中,直到可以弯曲为止。管子在成型后应立即老化。应指定压扁和慢弯试验,以确保连接管具有令人满意的延展性。
{"title":"Failure by Blowout of Aluminum Alloy 6061-T6 Connector Tubes From a Water-Cooling System","authors":"","doi":"10.31399/asm.fach.process.c0047080","DOIUrl":"https://doi.org/10.31399/asm.fach.process.c0047080","url":null,"abstract":"\u0000 Several of the aluminum alloy 6061-T6 drawn seamless tubes (ASTM B 234, 2.5 cm (1.0 in.) OD with wall thickness of 1.7 mm (0.065 in.)) connecting an array of headers to a system of water-cooling pipes failed. The tubes were supplied in the O temper. They were bent to the desired curvature, preheated, then solution treated, water quenched, and then aged for 8 to 10 h. Analysis (visual inspection, slow-bend testing, 65x macrographic analysis, macroetching, spectrographic analysis, hardness tests, microhardness tests, tension tests, and microscopic examination) supported the conclusions that bending of the connector tubes in the annealed condition induced critical strain near the neutral axis of the tube, which resulted in excessive growth of individual grains during the subsequent solution treatment. Recommendations included bending the connector tubes in the T4 temper as early as possible after being quenched from the solution temperature. The tubes should be stored in dry ice after the quench until bending can be done. The tubes should be aged immediately after being formed. Flattening and slow-bend tests should be specified to ensure that the connector tubes had satisfactory ductility.","PeriodicalId":294593,"journal":{"name":"ASM Failure Analysis Case Histories: Processing Errors and Defects","volume":"93 1","pages":"0"},"PeriodicalIF":0.0,"publicationDate":"2019-06-01","publicationTypes":"Journal Article","fieldsOfStudy":null,"isOpenAccess":false,"openAccessPdf":"","citationCount":null,"resultStr":null,"platform":"Semanticscholar","paperid":"121196428","PeriodicalName":null,"FirstCategoryId":null,"ListUrlMain":null,"RegionNum":0,"RegionCategory":"","ArticlePicture":[],"TitleCN":null,"AbstractTextCN":null,"PMCID":"","EPubDate":null,"PubModel":null,"JCR":null,"JCRName":null,"Score":null,"Total":0}
引用次数: 0
Fracturing of Gray Iron Door-Closer Cylinder Castings Caused by Lack of Foundry Control Over Chemistry 灰铸铁闭门筒铸件化学控制不足导致的断裂
Pub Date : 2019-06-01 DOI: 10.31399/asm.fach.process.c0047297
Door-closer cylinder castings manufactured of class 30 gray iron were breaking during machining. The manufacturing source reported that a random sampling of castings from this lot had hardnesses from 180 to 210 HRB. Based on the color of the components, heat treatment of these castings was suspected. Metallurgical examination on two representative castings supported the conclusions that the cracks in these gray iron door closers that were present either before or during the heat treatment were attributed to a substandard microstructure of the wrong type of graphite combined with excessive ferrite. This anomalous structure is caused by shortcomings in the foundry practice of chemical composition, solidification, and inoculation control. Judging from the microstructure, the strength of the material was lower than desired for class 30 gray iron, and the suspected heat treatment further reduced the strength. Recommendations included that the chemistry and inoculation should be controlled to produce type A graphite structure. The chemistry control should aim for a carbon equivalent close to 4.3% to achieve adequate fluidity for thin sections and to alleviate gas defects.
用30级灰铸铁制造的闭门缸铸件在加工过程中发生了断裂。制造来源报告说,这批铸件的随机抽样硬度在180到210 HRB之间。根据零件的颜色,怀疑这些铸件经过热处理。对两个有代表性的铸件进行的冶金检查支持以下结论:这些灰铸铁闭门器在热处理前或热处理过程中出现的裂纹是由于错误类型的石墨和过量的铁素体的不合格显微组织造成的。这种异常结构是由铸造实践中化学成分、凝固和孕育控制的缺陷造成的。从显微组织来看,材料的强度低于30级灰铸铁的要求,疑似热处理进一步降低了强度。建议包括控制化学和接种,以产生A型石墨结构。化学控制应以接近4.3%的碳当量为目标,以实现薄截面的足够流动性,并减轻气体缺陷。
{"title":"Fracturing of Gray Iron Door-Closer Cylinder Castings Caused by Lack of Foundry Control Over Chemistry","authors":"","doi":"10.31399/asm.fach.process.c0047297","DOIUrl":"https://doi.org/10.31399/asm.fach.process.c0047297","url":null,"abstract":"\u0000 Door-closer cylinder castings manufactured of class 30 gray iron were breaking during machining. The manufacturing source reported that a random sampling of castings from this lot had hardnesses from 180 to 210 HRB. Based on the color of the components, heat treatment of these castings was suspected. Metallurgical examination on two representative castings supported the conclusions that the cracks in these gray iron door closers that were present either before or during the heat treatment were attributed to a substandard microstructure of the wrong type of graphite combined with excessive ferrite. This anomalous structure is caused by shortcomings in the foundry practice of chemical composition, solidification, and inoculation control. Judging from the microstructure, the strength of the material was lower than desired for class 30 gray iron, and the suspected heat treatment further reduced the strength. Recommendations included that the chemistry and inoculation should be controlled to produce type A graphite structure. The chemistry control should aim for a carbon equivalent close to 4.3% to achieve adequate fluidity for thin sections and to alleviate gas defects.","PeriodicalId":294593,"journal":{"name":"ASM Failure Analysis Case Histories: Processing Errors and Defects","volume":"61 1","pages":"0"},"PeriodicalIF":0.0,"publicationDate":"2019-06-01","publicationTypes":"Journal Article","fieldsOfStudy":null,"isOpenAccess":false,"openAccessPdf":"","citationCount":null,"resultStr":null,"platform":"Semanticscholar","paperid":"115208502","PeriodicalName":null,"FirstCategoryId":null,"ListUrlMain":null,"RegionNum":0,"RegionCategory":"","ArticlePicture":[],"TitleCN":null,"AbstractTextCN":null,"PMCID":"","EPubDate":null,"PubModel":null,"JCR":null,"JCRName":null,"Score":null,"Total":0}
引用次数: 0
Ductile Overload Fracture of an Extension Ladder Made From 6061-T6 Aluminum Alloy Extrusions 6061-T6铝合金拉伸梯的延性过载断裂
Pub Date : 2019-06-01 DOI: 10.31399/asm.fach.process.c0046015
A two-section extension ladder, made from 6061-T6 aluminum alloy extrusions and stampings that were riveted together at each rung location and at the ends of side rails, broke in service after having been used at the sites of several fires by the fire department of a large city. The fracture surfaces were examined visually and by optical (light) stereomicroscopy. Material testing showed a sample to be within the specified material limits for aluminum alloy 6061. Microscopic examination showed no significant differences in microstructure or grain size among the four T-sections, and thickness measurements at various locations indicated that thicknesses were well within standard industry tolerances for aluminum extrusions in this size range. However, hardness testing of the four T-sections showed that in two, hardness was considerably lower than the acceptable hardness for the T6 temper and were within the range for 6061-T4 (acceptable hardness, 19 to 45 HRB). This indicated they had been naturally aged at room temperature after solution heat treatment instead of artificially aged as per specs. Edge cracking in two of the T-sections was the result of improper conditions during extrusion of the T-sections; however, this condition was not a primary cause of failure.
一个由6061-T6铝合金挤压件和冲压件在每个横档位置和侧轨末端铆接在一起的两段延伸梯,在被一个大城市的消防部门用于几次火灾现场后中断了使用。用视觉和光学立体显微镜检查断口表面。材料测试表明样品在铝合金6061规定的材料限制范围内。显微检查显示,四个t型段之间的显微组织和晶粒尺寸没有显著差异,不同位置的厚度测量表明,厚度完全在该尺寸范围内铝挤压件的标准工业公差范围内。然而,对四个t型断面的硬度测试表明,其中两个断面的硬度明显低于T6回火的可接受硬度,并且在6061-T4(可接受硬度,19至45 HRB)的范围内。这表明它们是经过固溶热处理后在室温下自然老化的,而不是按照规格进行人工老化的。其中两个t型型材的边缘开裂是由于t型型材挤压时条件不当造成的;然而,这种情况并不是失败的主要原因。
{"title":"Ductile Overload Fracture of an Extension Ladder Made From 6061-T6 Aluminum Alloy Extrusions","authors":"","doi":"10.31399/asm.fach.process.c0046015","DOIUrl":"https://doi.org/10.31399/asm.fach.process.c0046015","url":null,"abstract":"\u0000 A two-section extension ladder, made from 6061-T6 aluminum alloy extrusions and stampings that were riveted together at each rung location and at the ends of side rails, broke in service after having been used at the sites of several fires by the fire department of a large city. The fracture surfaces were examined visually and by optical (light) stereomicroscopy. Material testing showed a sample to be within the specified material limits for aluminum alloy 6061. Microscopic examination showed no significant differences in microstructure or grain size among the four T-sections, and thickness measurements at various locations indicated that thicknesses were well within standard industry tolerances for aluminum extrusions in this size range. However, hardness testing of the four T-sections showed that in two, hardness was considerably lower than the acceptable hardness for the T6 temper and were within the range for 6061-T4 (acceptable hardness, 19 to 45 HRB). This indicated they had been naturally aged at room temperature after solution heat treatment instead of artificially aged as per specs. Edge cracking in two of the T-sections was the result of improper conditions during extrusion of the T-sections; however, this condition was not a primary cause of failure.","PeriodicalId":294593,"journal":{"name":"ASM Failure Analysis Case Histories: Processing Errors and Defects","volume":"20 1","pages":"0"},"PeriodicalIF":0.0,"publicationDate":"2019-06-01","publicationTypes":"Journal Article","fieldsOfStudy":null,"isOpenAccess":false,"openAccessPdf":"","citationCount":null,"resultStr":null,"platform":"Semanticscholar","paperid":"125601142","PeriodicalName":null,"FirstCategoryId":null,"ListUrlMain":null,"RegionNum":0,"RegionCategory":"","ArticlePicture":[],"TitleCN":null,"AbstractTextCN":null,"PMCID":"","EPubDate":null,"PubModel":null,"JCR":null,"JCRName":null,"Score":null,"Total":0}
引用次数: 0
期刊
ASM Failure Analysis Case Histories: Processing Errors and Defects
全部 Acc. Chem. Res. ACS Applied Bio Materials ACS Appl. Electron. Mater. ACS Appl. Energy Mater. ACS Appl. Mater. Interfaces ACS Appl. Nano Mater. ACS Appl. Polym. Mater. ACS BIOMATER-SCI ENG ACS Catal. ACS Cent. Sci. ACS Chem. Biol. ACS Chemical Health & Safety ACS Chem. Neurosci. ACS Comb. Sci. ACS Earth Space Chem. ACS Energy Lett. ACS Infect. Dis. ACS Macro Lett. ACS Mater. Lett. ACS Med. Chem. Lett. ACS Nano ACS Omega ACS Photonics ACS Sens. ACS Sustainable Chem. Eng. ACS Synth. Biol. Anal. Chem. BIOCHEMISTRY-US Bioconjugate Chem. BIOMACROMOLECULES Chem. Res. Toxicol. Chem. Rev. Chem. Mater. CRYST GROWTH DES ENERG FUEL Environ. Sci. Technol. Environ. Sci. Technol. Lett. Eur. J. Inorg. Chem. IND ENG CHEM RES Inorg. Chem. J. Agric. Food. Chem. J. Chem. Eng. Data J. Chem. Educ. J. Chem. Inf. Model. J. Chem. Theory Comput. J. Med. Chem. J. Nat. Prod. J PROTEOME RES J. Am. Chem. Soc. LANGMUIR MACROMOLECULES Mol. Pharmaceutics Nano Lett. Org. Lett. ORG PROCESS RES DEV ORGANOMETALLICS J. Org. Chem. J. Phys. Chem. J. Phys. Chem. A J. Phys. Chem. B J. Phys. Chem. C J. Phys. Chem. Lett. Analyst Anal. Methods Biomater. Sci. Catal. Sci. Technol. Chem. Commun. Chem. Soc. Rev. CHEM EDUC RES PRACT CRYSTENGCOMM Dalton Trans. Energy Environ. Sci. ENVIRON SCI-NANO ENVIRON SCI-PROC IMP ENVIRON SCI-WAT RES Faraday Discuss. Food Funct. Green Chem. Inorg. Chem. Front. Integr. Biol. J. Anal. At. Spectrom. J. Mater. Chem. A J. Mater. Chem. B J. Mater. Chem. C Lab Chip Mater. Chem. Front. Mater. Horiz. MEDCHEMCOMM Metallomics Mol. Biosyst. Mol. Syst. Des. Eng. Nanoscale Nanoscale Horiz. Nat. Prod. Rep. New J. Chem. Org. Biomol. Chem. Org. Chem. Front. PHOTOCH PHOTOBIO SCI PCCP Polym. Chem.
×
引用
GB/T 7714-2015
复制
MLA
复制
APA
复制
导出至
BibTeX EndNote RefMan NoteFirst NoteExpress
×
0
微信
客服QQ
Book学术公众号 扫码关注我们
反馈
×
意见反馈
请填写您的意见或建议
请填写您的手机或邮箱
×
提示
您的信息不完整,为了账户安全,请先补充。
现在去补充
×
提示
您因"违规操作"
具体请查看互助需知
我知道了
×
提示
现在去查看 取消
×
提示
确定
Book学术官方微信
Book学术文献互助
Book学术文献互助群
群 号:481959085
Book学术
文献互助 智能选刊 最新文献 互助须知 联系我们:info@booksci.cn
Book学术提供免费学术资源搜索服务,方便国内外学者检索中英文文献。致力于提供最便捷和优质的服务体验。
Copyright © 2023 Book学术 All rights reserved.
ghs 京公网安备 11010802042870号 京ICP备2023020795号-1