Pub Date : 2019-06-01DOI: 10.31399/asm.fach.power.c9001456
An unusual type of defect was discovered during hydraulic testing of a water-tube boiler after repairs to the superheater tubes following erosion from soot-blowers. When the pressure reached 700 psi, slight leakage was found to be taking place from one of the superheater tubes in a region where there appeared to be a split, approximately 8 in. long. What was thought to be a split was actually a pronounced fold. Microscopic examination showed that a corrosion-fatigue fissure had developed from one of the inside corners of the fold, presumably as a result of the fluctuating bending stresses to which this portion of the tube would be subjected because of the discontinuity in the tube wall. It was from this fissure that the leakage occurred. It was evident that the defect developed during the manufacture of the tube, probably in the course of a drawing or rolling operation without an internal plug. The diam of this portion of the tube was reduced by local collapse and folding of the section rather than by longitudinal extension of the tube itself.
{"title":"An Unusual Defect in a Superheater Tube","authors":"","doi":"10.31399/asm.fach.power.c9001456","DOIUrl":"https://doi.org/10.31399/asm.fach.power.c9001456","url":null,"abstract":"\u0000 An unusual type of defect was discovered during hydraulic testing of a water-tube boiler after repairs to the superheater tubes following erosion from soot-blowers. When the pressure reached 700 psi, slight leakage was found to be taking place from one of the superheater tubes in a region where there appeared to be a split, approximately 8 in. long. What was thought to be a split was actually a pronounced fold. Microscopic examination showed that a corrosion-fatigue fissure had developed from one of the inside corners of the fold, presumably as a result of the fluctuating bending stresses to which this portion of the tube would be subjected because of the discontinuity in the tube wall. It was from this fissure that the leakage occurred. It was evident that the defect developed during the manufacture of the tube, probably in the course of a drawing or rolling operation without an internal plug. The diam of this portion of the tube was reduced by local collapse and folding of the section rather than by longitudinal extension of the tube itself.","PeriodicalId":107406,"journal":{"name":"ASM Failure Analysis Case Histories: Power Generating Equipment","volume":"1 1","pages":"0"},"PeriodicalIF":0.0,"publicationDate":"2019-06-01","publicationTypes":"Journal Article","fieldsOfStudy":null,"isOpenAccess":false,"openAccessPdf":"","citationCount":null,"resultStr":null,"platform":"Semanticscholar","paperid":"122581649","PeriodicalName":null,"FirstCategoryId":null,"ListUrlMain":null,"RegionNum":0,"RegionCategory":"","ArticlePicture":[],"TitleCN":null,"AbstractTextCN":null,"PMCID":"","EPubDate":null,"PubModel":null,"JCR":null,"JCRName":null,"Score":null,"Total":0}
Pub Date : 2019-06-01DOI: 10.31399/asm.fach.power.c0090181
Cracking in gas turbine blades was found to initiate from a mechanism of low-cycle fatigue (LCF). LCF is induced during thermal loading cycles in gas turbines. However, metallography of two cracked blades revealed a change in microstructure at as-cast surfaces for depths up to 0.41 mm (0.016 in.). Evaluation by SEM confirmed the difference in structure was associated with a lack of formation of coarse gamma prime structure in the matrix. Microhardness and miniature tensile test results indicated lower strength consistent with the absence of the coarse gamma prime constituent. The blade vendor found that the lot of hot isostatically pressed (HIP) blade castings had been exposed to an improper atmosphere during the HIP process, resulting in the weakened structure. Because subsequent failures were found in blades that did not come from the suspect HIP lot, the scope of the problem was considered generic, and the conclusion was that the primary failure mechanism was LCF. Material imperfections were a secondary deficiency that had the effect of causing the blades from the bad HIP lot to crack first.
发现燃气轮机叶片开裂是由低周疲劳机制引起的。LCF是在燃气轮机热负荷循环过程中产生的。然而,在深度达0.41 mm (0.016 in.)的铸态表面,两个裂纹叶片的金相分析显示微观结构发生了变化。扫描电镜分析证实,这种结构差异与基体中未形成粗γ prime结构有关。显微硬度和微观拉伸试验结果表明,强度较低,与缺乏粗γ基本成分一致。叶片供应商发现,许多热等静压(HIP)叶片铸件在HIP过程中暴露在不适当的气氛中,导致结构减弱。由于后续故障发生在并非来自可疑HIP批次的叶片中,因此该问题的范围被认为是通用的,结论是主要故障机制是LCF。材料缺陷是次要缺陷,它会导致来自不良HIP批次的叶片首先开裂。
{"title":"Cracking in Gas Turbine Blades","authors":"","doi":"10.31399/asm.fach.power.c0090181","DOIUrl":"https://doi.org/10.31399/asm.fach.power.c0090181","url":null,"abstract":"\u0000 Cracking in gas turbine blades was found to initiate from a mechanism of low-cycle fatigue (LCF). LCF is induced during thermal loading cycles in gas turbines. However, metallography of two cracked blades revealed a change in microstructure at as-cast surfaces for depths up to 0.41 mm (0.016 in.). Evaluation by SEM confirmed the difference in structure was associated with a lack of formation of coarse gamma prime structure in the matrix. Microhardness and miniature tensile test results indicated lower strength consistent with the absence of the coarse gamma prime constituent. The blade vendor found that the lot of hot isostatically pressed (HIP) blade castings had been exposed to an improper atmosphere during the HIP process, resulting in the weakened structure. Because subsequent failures were found in blades that did not come from the suspect HIP lot, the scope of the problem was considered generic, and the conclusion was that the primary failure mechanism was LCF. Material imperfections were a secondary deficiency that had the effect of causing the blades from the bad HIP lot to crack first.","PeriodicalId":107406,"journal":{"name":"ASM Failure Analysis Case Histories: Power Generating Equipment","volume":"18 1","pages":"0"},"PeriodicalIF":0.0,"publicationDate":"2019-06-01","publicationTypes":"Journal Article","fieldsOfStudy":null,"isOpenAccess":false,"openAccessPdf":"","citationCount":null,"resultStr":null,"platform":"Semanticscholar","paperid":"115851085","PeriodicalName":null,"FirstCategoryId":null,"ListUrlMain":null,"RegionNum":0,"RegionCategory":"","ArticlePicture":[],"TitleCN":null,"AbstractTextCN":null,"PMCID":"","EPubDate":null,"PubModel":null,"JCR":null,"JCRName":null,"Score":null,"Total":0}
Pub Date : 2019-06-01DOI: 10.31399/asm.fach.power.c0046966
A turbine vane made of cast cobalt-base alloy AMS 5382 (Stellite 31; composition: Co-25.5Cr-10.5Ni-7.5W) was returned from service after an undetermined number of service hours because of crack indications on the airfoil sections. This alloy is cast by the precision investment method. Analysis (visual inspection, 100x/500x metallographic examination of sections etched with a mixture of ferric chloride, hydrochloric acid, and methanol, and bend tests) supported the conclusions that cracking of the airfoil sections was caused by thermal fatigue and was contributed to by low ductility due to age hardening, subsurface oxidation related to intragranular carbides, and high residual tensile macrostresses. No further conclusions could be drawn because of the lack of detailed service history, and no recommendations were made.
{"title":"Failure of a Turbine Vane","authors":"","doi":"10.31399/asm.fach.power.c0046966","DOIUrl":"https://doi.org/10.31399/asm.fach.power.c0046966","url":null,"abstract":"\u0000 A turbine vane made of cast cobalt-base alloy AMS 5382 (Stellite 31; composition: Co-25.5Cr-10.5Ni-7.5W) was returned from service after an undetermined number of service hours because of crack indications on the airfoil sections. This alloy is cast by the precision investment method. Analysis (visual inspection, 100x/500x metallographic examination of sections etched with a mixture of ferric chloride, hydrochloric acid, and methanol, and bend tests) supported the conclusions that cracking of the airfoil sections was caused by thermal fatigue and was contributed to by low ductility due to age hardening, subsurface oxidation related to intragranular carbides, and high residual tensile macrostresses. No further conclusions could be drawn because of the lack of detailed service history, and no recommendations were made.","PeriodicalId":107406,"journal":{"name":"ASM Failure Analysis Case Histories: Power Generating Equipment","volume":"20 1","pages":"0"},"PeriodicalIF":0.0,"publicationDate":"2019-06-01","publicationTypes":"Journal Article","fieldsOfStudy":null,"isOpenAccess":false,"openAccessPdf":"","citationCount":null,"resultStr":null,"platform":"Semanticscholar","paperid":"116874824","PeriodicalName":null,"FirstCategoryId":null,"ListUrlMain":null,"RegionNum":0,"RegionCategory":"","ArticlePicture":[],"TitleCN":null,"AbstractTextCN":null,"PMCID":"","EPubDate":null,"PubModel":null,"JCR":null,"JCRName":null,"Score":null,"Total":0}
Pub Date : 2019-06-01DOI: 10.31399/asm.fach.power.c0048714
Tubes in heat exchangers, made of copper alloy C44300 and used for cooling air failed after 5 to six years of service. Air passed over the shell-side surface of the tubes and was cooled by water flowing through the tubes. Water vapor in the air was condensed (pH 4.5) on the tube surfaces during the cooling process. Air flow over the tubes reversed direction every 585 mm as a result of baffling placed in the heat exchangers. An uneven ridgelike thinning and perforation of the tube wall on the leeward side of the tube was revealed by visual examination. Undercut pits on the outer surface of the tube were revealed by metallographic examination of a cross section of the failed area. Impingement attack which led to perforation was revealed by both the ridgelike appearance of the damaged area and the undercut pitting. The heat exchanger was retubed with tubes made of aluminum bronze (copper alloy C61400).
{"title":"Failure of Copper Alloy 443 Heat-Exchanger Tubes","authors":"","doi":"10.31399/asm.fach.power.c0048714","DOIUrl":"https://doi.org/10.31399/asm.fach.power.c0048714","url":null,"abstract":"\u0000 Tubes in heat exchangers, made of copper alloy C44300 and used for cooling air failed after 5 to six years of service. Air passed over the shell-side surface of the tubes and was cooled by water flowing through the tubes. Water vapor in the air was condensed (pH 4.5) on the tube surfaces during the cooling process. Air flow over the tubes reversed direction every 585 mm as a result of baffling placed in the heat exchangers. An uneven ridgelike thinning and perforation of the tube wall on the leeward side of the tube was revealed by visual examination. Undercut pits on the outer surface of the tube were revealed by metallographic examination of a cross section of the failed area. Impingement attack which led to perforation was revealed by both the ridgelike appearance of the damaged area and the undercut pitting. The heat exchanger was retubed with tubes made of aluminum bronze (copper alloy C61400).","PeriodicalId":107406,"journal":{"name":"ASM Failure Analysis Case Histories: Power Generating Equipment","volume":"52 1","pages":"0"},"PeriodicalIF":0.0,"publicationDate":"2019-06-01","publicationTypes":"Journal Article","fieldsOfStudy":null,"isOpenAccess":false,"openAccessPdf":"","citationCount":null,"resultStr":null,"platform":"Semanticscholar","paperid":"126264170","PeriodicalName":null,"FirstCategoryId":null,"ListUrlMain":null,"RegionNum":0,"RegionCategory":"","ArticlePicture":[],"TitleCN":null,"AbstractTextCN":null,"PMCID":"","EPubDate":null,"PubModel":null,"JCR":null,"JCRName":null,"Score":null,"Total":0}
Pub Date : 2019-06-01DOI: 10.31399/asm.fach.power.c9001409
Dezincification is a particular form of corrosive attack which may occur in a variety of environments and to which some brasses are susceptible. It is favored by waters having a high oxygen, carbon dioxide, or chloride content, and is accelerated by elevated temperatures and low water velocities. In the present study, steam turbine condenser tubes had to be renewed after 25 years of service. The tubes were nominally of 70:30 brass. The appearance of a typically corroded one showed uniform dezincification attack on the bore, extending from one-half to two-thirds through the tube wall thickness.
{"title":"Dezincification of Brass Tubes in a Steam Turbine Condenser","authors":"","doi":"10.31399/asm.fach.power.c9001409","DOIUrl":"https://doi.org/10.31399/asm.fach.power.c9001409","url":null,"abstract":"\u0000 Dezincification is a particular form of corrosive attack which may occur in a variety of environments and to which some brasses are susceptible. It is favored by waters having a high oxygen, carbon dioxide, or chloride content, and is accelerated by elevated temperatures and low water velocities. In the present study, steam turbine condenser tubes had to be renewed after 25 years of service. The tubes were nominally of 70:30 brass. The appearance of a typically corroded one showed uniform dezincification attack on the bore, extending from one-half to two-thirds through the tube wall thickness.","PeriodicalId":107406,"journal":{"name":"ASM Failure Analysis Case Histories: Power Generating Equipment","volume":"129 1","pages":"0"},"PeriodicalIF":0.0,"publicationDate":"2019-06-01","publicationTypes":"Journal Article","fieldsOfStudy":null,"isOpenAccess":false,"openAccessPdf":"","citationCount":null,"resultStr":null,"platform":"Semanticscholar","paperid":"115007916","PeriodicalName":null,"FirstCategoryId":null,"ListUrlMain":null,"RegionNum":0,"RegionCategory":"","ArticlePicture":[],"TitleCN":null,"AbstractTextCN":null,"PMCID":"","EPubDate":null,"PubModel":null,"JCR":null,"JCRName":null,"Score":null,"Total":0}
Pub Date : 2019-06-01DOI: 10.31399/asm.fach.power.c9001711
J. A. Pero-Sanz, D. Plaza, M. Ruiz, J. Asensio, J. Verdeja
Failures of 10Cr-Mo9-10 and X 20Cr-Mo-V12-1 superheated pipes during service in steam power generation plants are described. Through micrographic and fractographic analysis, creep and overheating were identified as the cause of failure. The Larson-Miller parameter is computed, as a function of oxidation thickness, temperature and time, confirming the creep failure diagnostic.
介绍了蒸汽发电厂10Cr-Mo9-10和x20cr - mo - v12 -1过热管在使用过程中的故障。通过显微和断口分析,确定蠕变和过热是失效的原因。计算了拉尔森-米勒参数作为氧化厚度、温度和时间的函数,确定了蠕变失效诊断。
{"title":"Creep Failure Analysis of Steel Tubes","authors":"J. A. Pero-Sanz, D. Plaza, M. Ruiz, J. Asensio, J. Verdeja","doi":"10.31399/asm.fach.power.c9001711","DOIUrl":"https://doi.org/10.31399/asm.fach.power.c9001711","url":null,"abstract":"\u0000 Failures of 10Cr-Mo9-10 and X 20Cr-Mo-V12-1 superheated pipes during service in steam power generation plants are described. Through micrographic and fractographic analysis, creep and overheating were identified as the cause of failure. The Larson-Miller parameter is computed, as a function of oxidation thickness, temperature and time, confirming the creep failure diagnostic.","PeriodicalId":107406,"journal":{"name":"ASM Failure Analysis Case Histories: Power Generating Equipment","volume":"2 1","pages":"0"},"PeriodicalIF":0.0,"publicationDate":"2019-06-01","publicationTypes":"Journal Article","fieldsOfStudy":null,"isOpenAccess":false,"openAccessPdf":"","citationCount":null,"resultStr":null,"platform":"Semanticscholar","paperid":"128460894","PeriodicalName":null,"FirstCategoryId":null,"ListUrlMain":null,"RegionNum":0,"RegionCategory":"","ArticlePicture":[],"TitleCN":null,"AbstractTextCN":null,"PMCID":"","EPubDate":null,"PubModel":null,"JCR":null,"JCRName":null,"Score":null,"Total":0}
Pub Date : 2019-06-01DOI: 10.31399/asm.fach.power.c0091703
An arsenical admiralty brass (UNS C44300) finned tube in a generator air cooler unit at a hydroelectric power station failed. The unit had been in operation for approximately 49,000 h. The cooling medium for the tubes was water from a river. Air flowed over the finned exterior of the tubes, while water circulated through the tubes. Investigation (visual inspection, leak testing, history review, 100X micrographs etched in potassium dichromate, chemical analysis, and EDS and XRD analysis of internal tube deposits) supported the conclusion that the cause of the tube leaks was ammonia-induced SCC. Because the cracks initiated on the inside surfaces of the tubes and because the river water was not treated before it entered the coolers, the ammonia was likely present in the river water and probably concentrated under the internal deposits. Recommendations included either eliminating the ammonia (prohibitively expensive in cost and time) or using an alternate material (such as a 70Cu-30Ni alloy or a more expensive titanium alloy) that is resistant to ammonia corrosion as well as to chlorides and sulfur species.
{"title":"Stress-Corrosion Cracking of a Brass Tube in a Generator Air Cooler Unit","authors":"","doi":"10.31399/asm.fach.power.c0091703","DOIUrl":"https://doi.org/10.31399/asm.fach.power.c0091703","url":null,"abstract":"\u0000 An arsenical admiralty brass (UNS C44300) finned tube in a generator air cooler unit at a hydroelectric power station failed. The unit had been in operation for approximately 49,000 h. The cooling medium for the tubes was water from a river. Air flowed over the finned exterior of the tubes, while water circulated through the tubes. Investigation (visual inspection, leak testing, history review, 100X micrographs etched in potassium dichromate, chemical analysis, and EDS and XRD analysis of internal tube deposits) supported the conclusion that the cause of the tube leaks was ammonia-induced SCC. Because the cracks initiated on the inside surfaces of the tubes and because the river water was not treated before it entered the coolers, the ammonia was likely present in the river water and probably concentrated under the internal deposits. Recommendations included either eliminating the ammonia (prohibitively expensive in cost and time) or using an alternate material (such as a 70Cu-30Ni alloy or a more expensive titanium alloy) that is resistant to ammonia corrosion as well as to chlorides and sulfur species.","PeriodicalId":107406,"journal":{"name":"ASM Failure Analysis Case Histories: Power Generating Equipment","volume":"1 1","pages":"0"},"PeriodicalIF":0.0,"publicationDate":"2019-06-01","publicationTypes":"Journal Article","fieldsOfStudy":null,"isOpenAccess":false,"openAccessPdf":"","citationCount":null,"resultStr":null,"platform":"Semanticscholar","paperid":"129898034","PeriodicalName":null,"FirstCategoryId":null,"ListUrlMain":null,"RegionNum":0,"RegionCategory":"","ArticlePicture":[],"TitleCN":null,"AbstractTextCN":null,"PMCID":"","EPubDate":null,"PubModel":null,"JCR":null,"JCRName":null,"Score":null,"Total":0}
Pub Date : 2019-06-01DOI: 10.31399/asm.fach.power.c9001559
A. A. Stein, V. Zilberstein, W. S. Clancy, G. J. Davis
One inch diam Type 304 stainless steel piping was designed to carry containment atmosphere samples to an analyzer to monitor hydrogen and oxygen levels during operational and the design basis accident conditions that are postulated to occur in a boiling water reactor. Only one of six lines in the system had thru-wall cracks. Shallow incipient cracks were detected at the lowest elevations of one other line. The balance of the system had no signs of SCC attack. Chlorides and corrosion deposits in varying amounts were found throughout the system. The failure mechanism was transgranular, chloride, stress-corrosion cracking. Replacement decisions were based on the presence of SCC attack or heavy corrosion deposits indicative of extended exposure time to chloride-contaminated water. The existing uncracked pipe, about 75 percent of the piping in the system, was retained despite the presence of low level surface chlorides. Controls were implemented to insure that temperatures are kept below 150 deg F, or, walls of the pipe are moisture-free or the cumulative wetted period will never exceed 30 h.
{"title":"Recovery of a Type 304 Stainless Steel Piping System Contaminated with Chlorides","authors":"A. A. Stein, V. Zilberstein, W. S. Clancy, G. J. Davis","doi":"10.31399/asm.fach.power.c9001559","DOIUrl":"https://doi.org/10.31399/asm.fach.power.c9001559","url":null,"abstract":"\u0000 One inch diam Type 304 stainless steel piping was designed to carry containment atmosphere samples to an analyzer to monitor hydrogen and oxygen levels during operational and the design basis accident conditions that are postulated to occur in a boiling water reactor. Only one of six lines in the system had thru-wall cracks. Shallow incipient cracks were detected at the lowest elevations of one other line. The balance of the system had no signs of SCC attack. Chlorides and corrosion deposits in varying amounts were found throughout the system. The failure mechanism was transgranular, chloride, stress-corrosion cracking. Replacement decisions were based on the presence of SCC attack or heavy corrosion deposits indicative of extended exposure time to chloride-contaminated water. The existing uncracked pipe, about 75 percent of the piping in the system, was retained despite the presence of low level surface chlorides. Controls were implemented to insure that temperatures are kept below 150 deg F, or, walls of the pipe are moisture-free or the cumulative wetted period will never exceed 30 h.","PeriodicalId":107406,"journal":{"name":"ASM Failure Analysis Case Histories: Power Generating Equipment","volume":"1 1","pages":"0"},"PeriodicalIF":0.0,"publicationDate":"2019-06-01","publicationTypes":"Journal Article","fieldsOfStudy":null,"isOpenAccess":false,"openAccessPdf":"","citationCount":null,"resultStr":null,"platform":"Semanticscholar","paperid":"130412273","PeriodicalName":null,"FirstCategoryId":null,"ListUrlMain":null,"RegionNum":0,"RegionCategory":"","ArticlePicture":[],"TitleCN":null,"AbstractTextCN":null,"PMCID":"","EPubDate":null,"PubModel":null,"JCR":null,"JCRName":null,"Score":null,"Total":0}
Pub Date : 2019-06-01DOI: 10.31399/asm.fach.power.c9001448
Rivets from the longitudinal seam of the terminal shell ring of a 12 year old Lancashire boiler broke off easily during examination. Cleavage fractures indicated a brittle material. Microstructure of a sectioned rivet head was typical of a normal rimming steel except the ferrite crystals contained numerous nitride needles. Their existence indicated an abnormally high nitrogen content. If such a steel is heated for a lengthy period to a temperature of that prevailing in a boiler, precipitation of the nitrides may be expected, with consequent embrittlement. In this case, embrittlement of this type was the primary cause of the breaking off of the type rivet heads. Nothing was observed in the course of the examination that suggested caustic cracking.
{"title":"Aging of Boiler Rivets","authors":"","doi":"10.31399/asm.fach.power.c9001448","DOIUrl":"https://doi.org/10.31399/asm.fach.power.c9001448","url":null,"abstract":"\u0000 Rivets from the longitudinal seam of the terminal shell ring of a 12 year old Lancashire boiler broke off easily during examination. Cleavage fractures indicated a brittle material. Microstructure of a sectioned rivet head was typical of a normal rimming steel except the ferrite crystals contained numerous nitride needles. Their existence indicated an abnormally high nitrogen content. If such a steel is heated for a lengthy period to a temperature of that prevailing in a boiler, precipitation of the nitrides may be expected, with consequent embrittlement. In this case, embrittlement of this type was the primary cause of the breaking off of the type rivet heads. Nothing was observed in the course of the examination that suggested caustic cracking.","PeriodicalId":107406,"journal":{"name":"ASM Failure Analysis Case Histories: Power Generating Equipment","volume":"118 1","pages":"0"},"PeriodicalIF":0.0,"publicationDate":"2019-06-01","publicationTypes":"Journal Article","fieldsOfStudy":null,"isOpenAccess":false,"openAccessPdf":"","citationCount":null,"resultStr":null,"platform":"Semanticscholar","paperid":"133503530","PeriodicalName":null,"FirstCategoryId":null,"ListUrlMain":null,"RegionNum":0,"RegionCategory":"","ArticlePicture":[],"TitleCN":null,"AbstractTextCN":null,"PMCID":"","EPubDate":null,"PubModel":null,"JCR":null,"JCRName":null,"Score":null,"Total":0}
Pub Date : 2019-06-01DOI: 10.31399/asm.fach.power.c0048158
Several of the springs, made of 1.1 mm diam Inconel X-750 wire and used for tightening the interstage packing ring in a high-pressure turbine, were found broken after approximately seven years of operation. Intergranular cracks about 1.3 mm in depth and oriented at an angle of 45 deg to the axis of the wire were revealed by metallographic examination. A light-gray phase, which had the appearance of liquid-metal corrosion, was observed to have penetrated the grains on the fracture surfaces. The spring wires were found to fracture in a brittle manner characteristic of fracture from torsional loading (along a plane 45 deg to the wire axis). Liquid-metal embrittlement was expected to have been caused by metals (Sn, Zn, Pb) which melt much below maximum service temperature of the turbine. The springs were concluded to have fractured by intergranular stress-corrosion cracking promoted by the action of liquid zinc and tin in combination with static and torsional stresses on the spring wire. As a corrective measure, Na, Sn, and Zn which were present in pigmented oil used as a lubricant during spring winding was cleaned thoroughly by the spring manufacturer before shipment to remove all contaminants.
{"title":"Stress-Corrosion Cracking of Inconel X-750 Springs","authors":"","doi":"10.31399/asm.fach.power.c0048158","DOIUrl":"https://doi.org/10.31399/asm.fach.power.c0048158","url":null,"abstract":"\u0000 Several of the springs, made of 1.1 mm diam Inconel X-750 wire and used for tightening the interstage packing ring in a high-pressure turbine, were found broken after approximately seven years of operation. Intergranular cracks about 1.3 mm in depth and oriented at an angle of 45 deg to the axis of the wire were revealed by metallographic examination. A light-gray phase, which had the appearance of liquid-metal corrosion, was observed to have penetrated the grains on the fracture surfaces. The spring wires were found to fracture in a brittle manner characteristic of fracture from torsional loading (along a plane 45 deg to the wire axis). Liquid-metal embrittlement was expected to have been caused by metals (Sn, Zn, Pb) which melt much below maximum service temperature of the turbine. The springs were concluded to have fractured by intergranular stress-corrosion cracking promoted by the action of liquid zinc and tin in combination with static and torsional stresses on the spring wire. As a corrective measure, Na, Sn, and Zn which were present in pigmented oil used as a lubricant during spring winding was cleaned thoroughly by the spring manufacturer before shipment to remove all contaminants.","PeriodicalId":107406,"journal":{"name":"ASM Failure Analysis Case Histories: Power Generating Equipment","volume":"5 1","pages":"0"},"PeriodicalIF":0.0,"publicationDate":"2019-06-01","publicationTypes":"Journal Article","fieldsOfStudy":null,"isOpenAccess":false,"openAccessPdf":"","citationCount":null,"resultStr":null,"platform":"Semanticscholar","paperid":"133724555","PeriodicalName":null,"FirstCategoryId":null,"ListUrlMain":null,"RegionNum":0,"RegionCategory":"","ArticlePicture":[],"TitleCN":null,"AbstractTextCN":null,"PMCID":"","EPubDate":null,"PubModel":null,"JCR":null,"JCRName":null,"Score":null,"Total":0}